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NRC Seal NRC NEWS
U. S. NUCLEAR REGULATORY COMMISSION
Office of Public Affairs Telephone: 301/415-8200
Washington, DC 20555-001 E-mail: opa@nrc.gov

                               
  
  No. 96-55                             FOR IMMEDIATE RELEASE
                                    (Thursday, April 4, 1996)
  
  
  NOTE TO EDITORS:
  
  
     The Nuclear Regulatory Commission staff has issued the
  attached letter to Northeast Utilities (NU) requiring certain
  information, under oath or affirmation, before restarting its
  Millstone 3 nuclear power plant in Connecticut. 
  
     The NRC is taking this action based on preliminary
  results of a special inspection that has identified design
  and equipment deficiencies described in an enclosure to the
  letter.  The deficiencies are similar in nature to those at
  Millstone 1 and 2, both of which are in shut down. 
  
     Millstone 3 is required to submit to the NRC, seven days
  before restarting from its current refueling outage, actions
  taken to assure future operation will be conducted in
  compliance with its operating license, NRC regulations and
  final safety analysis report for the plant. 
  
     Millstone 1 and 2 also are required to provide similar
  information and operating assurance to the NRC before being
  able to restart.
  
                              #
  
  Attachments:
  As stated
    .
                              April 4, 1996
  
  
  Mr. Robert E. Busch
  President - Energy Resources Group
  Northeast Utilities Service Company
  P.O. Box 128
  Waterford, CT  06385
  
  Dear Mr. Busch:
               
  On March 7, 1996, the NRC issued to Northeast Utilities (NU)
  a letter describing its review of an internal NU document,
  "ACR 7007 - Event Response Team Report" (7007 Report), dated
  February 22, 1996 and requesting additional information on
  NU's actions and plans to address the conclusions of the 7007
  Report as it pertains to Millstone Unit 3 and Haddam Neck. 
  At the time we issued that letter, we did not have a recent
  inspection history or findings with regard to Millstone Unit
  3 that revealed design deficiencies similar in number and
  nature to those of Millstone Units 1 and 2, but the 7007
  Report identified the potential for similar configuration
  management conditions at Millstone Unit 3.
  
  Since the March 7, 1996 letter, the NRC has initiated a
  special inspection at Millstone Unit 3.  Based on the
  preliminary results of the portion of the special inspection
  conducted to date, we have identified programmatic issues and
  design deficiencies at Millstone Unit 3 that are similar in
  nature to those at Millstone Units 1 and 2.  Examples of some
  of the deficiencies found in the special inspection are
  described in the enclosure to this letter.  In addition, you
  have recently identified design deficiencies in the auxiliary
  feedwater containment isolation valves and the recirculation
  spray system that have existed for more than 10 years.
  
  These findings raise substantial questions as to whether the
  Millstone Unit 3 facility is being operated and maintained in
  conformance with the updated final safety analysis report
  (UFSAR), license conditions, and Commission regulations. 
  Therefore, the NRC requires additional information to be
  submitted pursuant to Section 182a of the Atomic Energy Act
  of 1954, as amended, and 10 CFR 50.54(f) in writing, under
  oath or affirmation, to determine whether or not the license
  for Millstone Unit 3 should be suspended, modified, or
  revoked.  The information is to be submitted no later than 7
  days prior to Millstone Unit 3 restart (prior to criticality)
  from its current outage and is to describe actions taken to
  ensure that future operation of Millstone Unit 3 will be
  conducted in accordance with the terms and conditions of the
  Millstone Unit 3 operating license, the Commission's
  regulations, including 10 CFR 50.59, and the Millstone Unit 3
  UFSAR.  This request for information supercedes our previous
  request of March 7, 1996.
  Your submittal should describe actions taken to ensure that
  design and configuration control deficiencies at Millstone
  Unit 3 have been identified, and have been evaluated with
  regard to plant operability, the existence of unreviewed
  safety questions, and reportability.  Your submittal should
  also address your corrective actions.  In particular,
  seriously degraded conditions must be reported pursuant to 10
  CFR 50.72(b)(2)(i) and 50.73(a)(2)(ii).  Further, prior to
  restart of Millstone Unit 3, you must resolve, to the NRC's
  satisfaction, the issues raised in the examples described in
  the enclosure, the Auxiliary Feedwater valve issues, and the
  recirculation spray system matter.  We also recognize that
  ongoing activities by your staff as well as the NRC staff may
  identify additional issues which warrant resolution prior to
  restart.   
  
  In accordance with 10 CFR 2.790 of the NRC's "Rules of
  Practice," a copy of this letter and your responses will be
  placed in the NRC Public Document Room, the Gelman Building,
  2120 L Street, NW., Washington, DC, and in the local public
  document room located at the Learning Resources Center, Three
  Rivers Community-Technical College, 574 New London Turnpike,
  Norwich, Connecticut, and in the temporary public document
  room located at the Waterford Library, Waterford,
  Connecticut.  
  
                         Sincerely,
  
                         (original signed by W. T. Russel)
  
                         William T. Russell, Director
                         Office of Nuclear Reactor Regulation
  
  Enclosure:  Preliminary Inspection
            Findings
  
    .               PRELIMINARY INSPECTION FINDINGS
  
  
  Inoperability of the turbine-driven AFW pump during startup
  and shutdown
  
  In response to plant information report (PIR) 3-94-060, "AFW
  High Energy Line Break Concerns," dated March 15, 1994, the
  licensee developed a procedure to isolate the turbine-driven
  auxiliary feedwater (AFW) pump whenever either of the motor-driven AFW pumps were used for steam generator water level
  control (low power operations during startup or shutdown). 
  Technical Specification 3.7.1 requires operability of both
  motor-driven and the turbine-driven auxiliary feedwater pumps
  whenever the plant is in modes 1, 2, and 3.  
  
  Failure to remove plastic shipping plugs from Rosemount
  transmitters
  
  The NRC team observed two Rosemount transmitters, 3CHSFT139
  and 3CCPFT12B, with plastic shipping plugs installed, and
  transmitter 3GWSFT84 open at the alternate conduit entry
  point, contrary to the manufacturer's instructions to
  environmentally seal these openings with a stainless steel
  plug.  The licensee subsequently identified two safety-related and 94 non-safety related transmitters that required
  corrective action based on partial inspection.  The licensee
  had not completed inspection of the transmitters inside
  containment.
  
  Failure to correct degraded non-safety battery
  
  The NRC team found that the maintenance history on battery
  301D-1 demonstrated marginal capacity because the monthly
  surveillances were preceded by equalizing charges on eight
  occasions in 1995.  Although the battery is classified as
  non-safety, procedure AOP-3563 cautions the operators that a
  manual reactor trip is required upon the loss of the
  associated DC bus.  This DC bus is relied upon for the
  operation of all four steam generator atmospheric dump
  valves, and to provide control power for the 4160 volt
  emergency bus feeder breakers. 
  
  Inadequate Control of Modification of the service water
  system 
  
  A temporary modification was installed in 1990 that bypassed
  the automatic service water booster pump start on high
  discharge temperature in the MCC/rod control area room cooler
  ducts.  The safety evaluation performed was inadequate in
  that it did not address the substitution of a manual action
  for an automatic function and it did not address the deletion
  of an automatic start feature.  In addition, the licensee did
  not maintain a special instruction in an alarm response
  procedure required by the original bypass as a compensatory
  measure.  
  
  Potential introduction of foreign material into the
  containment sump 
  
  Test flange rings were installed on the recirculation system
  (RSS) suction piping penetrations in the containment sump by
  a modification in June 1995 (PDCR 3-94-0162).  The licensee
  installed bolts "snug tight" in the flange holes to prevent
  thread damage and minimize the accumulation of water and
  debris in the test ring bolt holes during plant operation. 
  This practice unnecessarily introduces material into the
  containment sump that could, if the bolts are dislodged or
  improperly controlled, be pulled into the suction of the RSS
  pumps and result in pump damage.