(TR 26, 90). In September or October 1991, the Complainant attended a meeting
arranged by Jim Spadafore with Carl Terry, Rick Abbott, and Mike Jones. (TR 93). In
November the Complainant received a letter from Matt Yeminy regarding the RHR system.
(RX-1).
The Complainant then met with Mr. Korcz about the Unit 2
licensing basis in regards to this issue. (TR 94). It was the Complainant's impression Mr. Korcz
was in full agreement with his position. (TR 95).
In December 1991 the Complainant had a conversation with
Richard Abbott, Unit 2 engineering manager, about the PR. It was Mr. Abbott's contention that
the issue was fully resolved and there was nothing more his department was going to do. Further
he told Complainant that nuclear engineers were going to be fired if they didn't do what they
were supposed to do. He said what they were supposed to do was what he told them to do. He
reminded Complainant he was a nuclear engineer and he was supposed to allow the PR to be
closed without objecting another time. (TR 28).
The Complainant told Jim Spadafore that engineering was not
going to do anymore work on the issue. The PR was closed soon after. (TR 96-97). The
Complainant stated that Mr. Terry had directed Jim Spadafore to close the PR. (TR 97).
In the fall of 1993 the Complainant re-raised the RHR issue
because of an inconsistency with the licensing basis and the regulations contained in the NRC
Regulation Guide Section 1.1393 pertaining to the RHR system and shutdown cooling. (see
CX-2,3). (TR 33-34). Section C of 1.1393 described a cold shutdown within 36 hours. The
method
in place, the Complainant said, would have exceeded 54 hours. (TR 35).
On December 22, 1993 the Complainant initiated a Deviation
Event Report ("DER"), which replaced problem reports, to reopen his concern on the
RHR system. This DER was approved by his supervisor. (TR 37). The Complainant heard from
operational engineering and the nuclear generation department that the problem belonged to
nuclear engineering. The DER was then forwarded to Mr. Brezina from nuclear engineering.
(TR 38). Mr. Brozina contacted the Complainant in January 1994 to discuss the problem. (TR
38).
It was the Complainant's opinion that the company preferred to
[Page 6]
have an emergency shutdown system that took 54 hours or longer to cool (as opposed to 36
hours). Because the reactor vessel was of only a certain thickness, it would be subject to thermo-
stratification if cooling took place faster than 1000 per hour. (TR 134-135).
Thermo-stratification occurred when the temperature at the top of the vessel was much higher
than the
bottom causing thermo-stress cracking of the vessel. This would be expensive to repair. (TR
135).
It was the Complainant's position that writing a procedure without
doing a safety evaluation would not have solved the problem. (TR 218). Engineering thought
there was no deviation present. (TR 219). Mr. Spadafore noted that he did not know if a safety
evaluation of the deviating alternate cooling system had ever been done. (TR 215).
Mr. Abbott reviewed the PR and agreed with his staff's initial
disposition of the PR (they were within the requirements of the FSAR). (TR 229). Abbott spoke
with Jim Spadafore and Complainant about the PR. (TR 230). He sent the PR back to
Complainant with a letter written by Matt Yeminy and Ken Korcz (RX-1) explaining their
rationale. (TR 229). Mr. Abbott concurred with the contents of that letter. (TR 230).
If an initiator of a PR/DER did not agree with the dispositioner he
could go to the line management of the organization responding to PR/DER, or go up his own
chain of command, or jump the chain to the vice president, or go to the Quality First Program, or
to the NRC. All of these options were available in 1991. (TR 233).
Mr. Abbott suggested to Jim Spadafore that he take the problem to
Mr. Terry and have him evaluate the issue. (TR 233). Eventually Gary Thompson signed-off the
PR. (TR 234). Mr. Thompson was the general supervisor of system engineering in the nuclear
generation department. It was his job to keep track of open and closed PRs. (TR 235).
Mr. Abbott stated there was a safety evaluation in place for the
operating procedure. However, he did not recall showing the safety evaluation to Jim Spadafore
or the Complainant. (TR 248).
Mr. Abbott did not specifically recall any discussion with the
Complainant about firing nuclear engineers in the hallway of P building or R building. (TR 242,
244). He said he never gave the Complainant any direction to close the PR. (TR 243). He
explained that he did not have the authority to tell him to close the PR. (TR 243). He maintained
he had no management authority over the Complainant.
Mr. O'Brien reviewed Complainant's PR (CX-1) in August or
September 1994. (TR 257). His supervisor had asked him to look at the whole package, the
corrective actions that had been taken as a result of the DER, and to give him an engineering
judgement if everything looked satisfactory. (TR 258).
Corrective action had been taken in response to the DER. (TR
[Page 7]
258). A new special operating procedure was written addressing the issues in the DER (reaching
cold shutdown in 36 hours). (TR 259).
It was Mr. O'Brien's opinion that the issues stated in Complainant's
PR were valid. (TR 260).
Mr. Terry had no direct role in the 1991 PR. (TR 302). He was
aware of the PR (CX-1) via information reports from ISEG and discussions with Jim Spadafore.
(TR 303). He had also talked to Rick Abbott about the PR. (TR 304). He had no direct
discussion with Complainant about the RHR. He did not give Jim Spadafore any directions
about disposing or closing the PR. (TR 305). The PR had no impact on safe operation. They had
a method to apply alternate shutdown cooling. (TR 305). The PR did not suggest they were out
of compliance with the technical specifications.
The DER (CX-4) was a different issue because it identified a
possible conflict with the regulatory guide. (TR 307). He became aware of the DER through the
Q1P in March 1994. (TR 307).
On cross-examination, Mr. Terry stated that an operating procedure
was written after Complainant was discharged and after he reported the issue to the NRC and
Quality 1st Program,. (TR 317). Mr. Terry disagreed with Jim Spadafore and Pat O'Brien when
they stated there was no safety evaluation for the shutdown system in 1991. (TR 318).
Safety Review and Audit Board
The second safety issue identified by the Complainant concerned
the disposition of Safety Operating Reports.
The Safety Review and Audit Board ("SRAB") was
made up of senior managers and outside contractors. The committee was headed by either Carl
Terry, the Vice-President of Nuclear Engineering, or Ralph Sylvia, the Executive Vice-President
of Nuclear Engineering. (TR 39). The Complainant was appointed to a SRAB subcommittee in
1993 by Jim Spadafore. (TR 39). The subcommittee was made up of four members: the
Complainant, Jim Spadafore, Walter D'Ardenne (GE Contractor), and Pat O'Brien. (TR 135).
The Respondent had in place a method to analyze and disposition
operating experience reports ("OER"). (TR 40). The Complainant's subcommittee
reviewed a 20% sample of OERs closed during a certain time frame. (TR 42). The group
prepared a report and presented it to the SRAB committee in the fall of 1993. Jim Spadafore,
chairman of the subcommittee, presented the general findings and the Complainant presented the
specific issues. (TR 115). The report had been reviewed and approved by all subcommittee
members. (see CX-5). The general conclusion from the report was that 25% of the issues were
not properly addressed. (TR 43).
[Page 8]
Mr. Terry was present at the SRAB meeting when the report from
the subcommittee was made. (TR 137). Mr. Terry specifically commented on an offgas event
and reactor vessel inaccuracies. Mr. Terry disagreed with their conclusions. (TR 138).
Mr. Burton had disagreed with some of the issues that were being
identified as being in error. (TR 205). A verbal presentation of the report was given to the SRAB
committee.
On cross-examination, Mr. Spadafore stated that other reports of
the subcommittee identified shortcomings and inadequate actions to the same extent as the
September 1993 report. (TR 219). Mr. Terry was not angry because the report identified DERs
that had not been handled properly. (TR 220).
Mr. Terry was the chairman of the SRAB committee. His main
concern over the subcommittee's report (CX-5) was that there was no resolution between the
branch manager of QA and the ISEG people over whether the findings were valid or not. (TR
310-311). He was upset over their lack of preparation. (TR 312).
One particular event was an "offgas fire". In the
reactor, gases from the turbine are radioactive and can not be released into the atmosphere.
Instead they are forwarded into an offgas system which retains the radioactivity by using
charcoal beds until it is decayed to a point it can be safely released. (TR 43).
The Complainant testified it was widely known in the industry that
this system was very susceptible to a fire in the first train of a charcoal bed. (TR 43). There were
many OERs pertaining to this issue. There was an offgas fire at Nine Mile in the summer of
1993. This was a widely known, industry known, incident. (TR 44). The NRC investigated on
site. (TR 44).
Someone other than Complainant conducted a root cause
investigation after the event and concluded the present DER system would prevent such an event
from happening again. (TR 46). However, Complainant discovered that a DER involving offgas
fires had been closed out 2 months before the incident. (TR 47). The Complainant concluded the
present DER system contained problems in its performance that would miss industry issues.
(CX-5).
The incident needed to be reviewed by the Site Operation Review
Committee ("SORC"), but by the closure of the DER and assigning it to another one,
the SORC review would have been missed. (TR 48). It was the plant manager's responsibility to
decide if it should go to SORC. (TR 49).
Another issue raised by the Complainant concerns the
Containment Spray System. The Complainant was assigned by Jim Spadafore to do a special
assignment for SORC. (TR 50). This assignment concerned a safety evaluation of a Unit 1
[Page 9]
containment spray system, specifically the water seal on that system. (TR 51). The said safety
evaluation had repeatedly come back for additional SORC reviews because of safety issues that
had been left out. At the time they were on revision 9 or higher. (TR 51). Safety evaluations
were performed in accordance with 10 C.F.R. § 50.59. (CX-2).
The Complainant created a report cataloging problems that should
have been addressed in a safety evaluation. (CX-6, 6a). The general conclusion of the report was
that the safety review process definitely needed improvement. (TR 55). The Complainant made
suggestions for improvements. (TR 55-56). Mr. O'Brien also signed the report. (TR 120).
Nuclear engineering of Unit 1 was responsible for the redone safety evaluations and was the
overall responsibility of Carl Terry. (TR 56).
Complainant stated his work responsibilities were different than
other ISEG engineers in that he looked into adverse performance in programs which indicated a
poor performance on managing the plant. (TR 56). He was assigned those responsibilities by Jim
Spadafore. (TR 57).
Mr. O'Brien was asked by Jim Spadafore to look into a matter
involving a water seal. The safety evaluation kept coming back to SORC and had to be revised.
(TR 251). He was assigned as lead for the investigation. (TR 251). The Complainant looked at
more of the technical aspects of the safety evaluation where O'Brien was looking at the
programmatic aspects. (TR 252). Two reviewers looked over their report and did not make any
significant changes. (TR 252-253). Before the report was issued, he had a discussion with some
of his peers in the licensing department. Lee Klosowski acted as the moderator. (TR 253).
O'Brien would not characterize the discussion as heated. (TR 254).
These activities are evidence of the Complainant's raising
important safety issues. It is his position that these concerns are especially important because
they influence overall site operations.
There was testimony by others about investigations by other ISEG
engineers. This was presented by the Respondent to attempt to prove that the complaints raised
by the Complainant were no different that those raised by other ISEG engineers.
Thomas Egan had been an ISEG engineer for 6 years. During that
time he filed a half dozen PRs. (TR 148). Some issues raised by Mr. Egan included: a PR
questioning the condition of equipment, tubing that was not capped off, performed safety
assessment after an off-site power loss in March 1992, and was presently looking at putting
breakers in cubicles. (TR 148-149). Mr. Egan encountered resistance from managers when
raising some issues. (TR 150). He had gotten into shouting matches with some managers. (TR
150). However, he did not have any difficulty working with those same individuals after the
incidents. (TR 151). Overall he said, the ISEG engineers would raise the same type of issues.
(TR 152).
[Page 10]
Mr. Spadafore stated that the filing of a PR or DER was not an
unusual occurrence. (TR 216). Other ISEG engineers filed PRs and DERs. (TR 216). There was
no difference in the nature of issues identified or pursued by the Complainant relative to issues
identified or pursued by other ISEG engineers. The problems raised with systems were to no
greater extent than anyone else in the group. (TR 217).
Mr. O'Brien had filed 10-15 DERs and couple dozen PRs. (TR
261). As a whole everything was about equal concerning the significance of problems raised by
the ISEG engineers. (TR 263).
For example, there had been a fuel bundle incident while preparing
for refueling at the end of 1991 or early 1992. ISEG was asked by the plant manager to conduct
a root cause investigation. Mr. O'Brien was one of the investigators along with Mr. Darweesh.
(TR 255). The incident was significant from a regulator point of view. (TR 255). However it
was not considered a significant safety issue. (TR 256).
Mr. O'Brien's report was critical of supervisory staff oversight in
that it was not what it should have been considering the job. Maintenance management should
have been more involved in providing oversight. A near miss had occurred a few days prior that
had not been communicated to the shift where the actual accident occurred. This could have
been significant in heightening awareness to human error. (TR 256). Mr. O'Brien did not receive
any negative criticism from management following the issuance of his report. (TR 257).
Issue
This case concerns the Complainant's firing by the Respondent.
The Complainant contends he was fired because he raised safety issues that were not adequately
addressed by management. The Respondent says the Complainant was fired as part of an overall
downsizing that was carried out according to written criteria.
Rightsizing
The Respondent began to cut staff in 1993 in order to make itself
competitive with other deliverers of power. The downsizing called "rightsizing" by
the Respondent was to be accomplished in two stages. In each stage only the employees with the
lowest performance evaluations were to be considered as expendable. The first stage in 1993
targeted the lowest 20%. The nuclear engineers were not targeted at all that year, so it did not
affect the Complainant. The second stage of the program in 1994 targeted the lowest 40% as
determined by performance evaluation. As nuclear engineers were targeted those engineers rated
in the lowest 40% by their supervisors should have been targeted. once a person was identified as
being in the lower 40% his name was sent to a Review Panel for further determination.
In addition to the published targeting program there are also
references to an ISEG rotation and elimination of jobs. There is no written documentation for
[Page 11]
either.
In 1993, the Complainant was told he was ranked in the lower 20%
of ISEG. (TR 124). He was not laid off in 1993. Jim Spadafore had been asked by the review
board to evaluate certain names against the Complainant. (TR 125). After the evaluation, the
Complainant was still considered to be the best qualified to hold an ISEG position, so he was
retained in the group. (TR 126).
In January 1994 a letter from B. Ralph Sylvia (CX-7) was issued
and distributed through company mail outlining how the down-sizing process would take place.
The Complainant had a conversation with Jim Spadafore about the cuts in January 1994. (TR
59). It was revealed cuts were going to be made in ISEG. (TR 59). Three engineering positions
associated with Unit I would be totally eliminated. (TR 59). One position would be eliminated
out of the 6 remaining. (TR 60). Unit 2's technical specifications required 5 full-time engineers.
As of January 1, 1994 there were 5 full-time engineers in Unit 2 ISEG. (TR 60). Unit 1 was not
required, as part of their licensing base, to have ISEG. Plants built after the Three-Mile Island
incident were required to have ISEG, those built before were grandfathered. As a result of the
cuts, Unit 1's ISEG was eliminated. (TR 61).
ISEG rotation was first mentioned at a group meeting with Jim
Spadafore. He explained that it would be a learning experience for the group. An ISEG engineer
would be taken out of his position and put into a position that he was reviewing to gain
experience in the day-to-day activities of that department. At the end of a year the engineer
would be rotated back to his own position. (TR 63). At the end of January 1994, the
Complainant was told he would be included in the ISEG rotation. (TR 64). However, the
Complainant had not seen a written plan or timetable for the rotation. (TR 128). It was Jim
Spadafore's impression that the rotation program would not result in any termination by the
right-sizing review board. (TR 64). Jim Spadafore had said Carl Terry was directing the rotation
plan.
(TR 128).
Mr. Sylvia testified about downsizing. After meeting with the
NRC resident inspector, Mr. Sylvia wanted to enhance the ISEG function. (TR 163). Senior
management received input from Jim Spadafore. A decision was made by the senior
management team in late February, early March to rotate the ISEG engineers. (TR
179). It was thought that employees would gain alot more experience through a rotation
program. However no timetable was adopted for ISEG rotation. They did not talk at all about
individual engineers. They did talk about rotating the manager. (TR 164). Mr. Sylvia spoke
with Patrick O'Brien in February 1994 about the ISEG rotation. (TR 176). Mr. O'Brien's name
was sent to the Review Board. (TR 177). The Board decided not to rotate people because they
were having enough trouble finding positions for people in the upper 60 percent. (TR 181).
Mr. Terry was involved in discussions regarding rotation of ISEG
engineers in early 1994. (TR 279-280). Jim Spadafore, in a presentation to senior management
mentioned he would like to see a rotation program established for ISEG. (TR 280). Rotation
[Page 12]
would not have involved a reduction of positions but rather people just changing jobs. (TR 281).
There was no timetable or written document outlining the rotation program. (TR 281).
There was much testimony about the downsizing process.
Testimony of Complainant
The Complainant was told by Jim Spadafore that he was not on the
40% list. (TR 61). The Complainant was told he was one person off the 40% list. (TR 62, 126).
On February 15, 1994 the Complainant was told, in a meeting with
Jim Spadafore and Thomas Egan, that he was terminated. (TR 62). He was no longer on site and
would be placed in a 2 month transition program. (TR 62). Again Jim Spadafore stated the
Complainant was not on the 40% list and that his position had not been eliminated. (TR 63).
The Complainant received a letter from Kathy Miles (CX-8) which
stated that his position had been abolished. The Complainant wrote back to Ms. Miles because
her letter was contrary to what Jim Spadafore had told him. (TR 67). The Complainant never
received a response from Ms. Miles. (TR 67).
The Complainant then wrote a letter (CX-10) to B. Ralph Sylvia,
Vice-President of Nuclear Engineering. Mr. Sylvia wrote back to Complainant (CX-11) and
indicated that the Complainant was not on the 40% list and that he was included in the ISEG
rotation program. (TR 69). After the Complainant left Niagara Mohawk, no rotation program
was ever implemented. (TR 69).
The Complainant had received management training in 1993. (TR
69). Also a computer printout of what training programs Complainant was submitted at the
hearing (CX-12).
Testimony of Thomas Egan
Mr. Egan attended the meeting with Jim Spadafore when the
Complainant was terminated. (TR 146). At that meeting Jim Spadafore told the Complainant he
was not on the 40% list. (TR 147). The 40% list was developed by departments for people who
were to be considered for release through "rightsizing." (TR 147). Complainant was
qualified as an ISEG engineer and was very good with computers. (TR 147).
Prior to the cuts in 1994, there were 5 degreed engineers for Unit 2
plus Jim Spadafore and 3 individuals at Unit 1 for a total of 9 employees. After the cuts there
were 4 engineers plus the manager. (TR 152-153). ISEG was down-sized by one engineer.
Respondent was required by the licensing base for Unit 2 to have 5
degreed engineers. (TR 154). Management functions had been given to one of those engineers.
[Page 13]
Therefore, it was the manager who was eliminated and not one of the engineers. (TR 154).
Darshan Suri was a good engineer and had a professional
engineering license. In addition, Mr. Suri was a better communicator than the Complainant. (TR
151). If Egan was to select who to cut, looking at the needs of ISEG he would have kept
Complainant, looking at the needs overall he would have chosen to keep Mr. Suri. (TR 153).
Testimony of Ralph Sylvia
The review board was developed jointly by the Director of Human
Resources and other members of the senior management team. (TR 168). There was an appeal
process for employees. He was the final step in the process. (TR 169). He received an appeal
from Complainant. (TR 169; CX-10). He had asked the Director of Human Resources, Mr.
Krueger, to look into the Complainant's case. (TR 170). Mr. Krueger prepared the response letter
(that Mr. Sylvia signed) to Complainant. (TR 170; CX-11).
Testimony of Jim Spadafore
Mr. Spadafore received a copy of Management Assessment
Process for 1994 (CX-15, CX-16) in late December, early January. (TR 209). Mr. Spadafore
used these documents in implementing the rightsizing process in his department. (TR 212). Mr.
Spadafore was instructed to verbally inform employees whether or not they were on the 40% list.
(TR 213). Mr. Spadafore told Complainant he was not on the 40% list. (TR 212). He did not tell
him he was one off the 40% list. (TR 213).
At a meeting on February 15, 1994, the Complainant was
terminated. Again Mr. Spadafore told the Complainant he was not on the 40% list. (TR 213).
Jim told the Complainant somebody else put him on the 40% list. His paperwork had been
received by the Review Board and they identified him to be on the 40% list. Prior to submitting
the Complainant's name to the Review Board, Spadafore told the Complainant that his name was
going to the Review Board for rotation pursuant to ISEG rotation. (TR 214).
In a special assessment, Mr. Spadafore had rated the Complainant
above Mr. Suri. The Complainant was let go, Suri was retained. (TR 224).
Mr. Spadafore testified that the ISEG rotation had not yet been
adopted at Unit 2. (TR 215). It has never been implemented.
Testimony of Richard Abbott
Mr. Abbott was on the review board that addressed rightsizing
issues. (TR 238). In 1994 there were two review boards in place that operated in parallel. (TR
239). Mr. Terry was on the same review board as Mr. Abbott. The review board discussed the
[Page 14]
Complainant and voted for transition. (TR 240). They also voted on Mr. Suri. (TR 240). The
board voted by secret ballot, Human Resources tallied the results. (TR 240). There was no
discussion of the rotation process. (TR 241).
However, in a senior management team meeting in December or
January, prior to the Review Board, ISEG rotation was discussed. A timetable was not adopted.
There was no discussion about individuals to be rotated. (TR 241).
On cross-examination Mr. Abbott stated that in 1992 he sat on a
Review Board and had one vote in deciding whether or not to terminate Complainant. (TR 245).
As a result of his vote Complainant no longer had a job. (TR 246).
Testimony of Patrick O'Brien
Jim Spadafore advised Mr. O'Brien that his name had been
submitted to the review board in December 1993 or January 1994. (TR 264). There had been
talk of rotating ISEG engineers and that the process was going to be handled through the
rightsizing review board. (TR 264). Mr. O'Brien was very concerned about his name being on
the list to go to the review board. (TR 265). He was afraid there would be no differentiation
between his name and others (least adequate performers) on the list. (TR 265). He wrote a letter
to Mr. Sylvia and had a meeting.' (TR 266). He believed Mr. Suri also had met with Mr. Sylvia.
He wanted to take whatever steps were necessary to get his name off of the list. (TR 266). The
list did not have rankings. (TR 267). There was no delineation between the 40% list and those in
the ISEG rotation. (TR 269). He believed Mr. Sylvia spoke with someone on the review board,
but did not know for sure. (TR 274).
Testimony of Paul Terry
Mr. Terry chaired the 1993 and 1994 review committees that were
established to examine people for rightsizing. (TR 282). Senior management made up the review
board. (TR 286). In 1993 they cut 10% of the management workforce. However, their goal was
to retain the best people. (TR 282). They reviewed those people whose jobs were abolished and
those on a lower performance level. (TR 283).
In 1993 Complainant's name was before the review board because
he was in the lower 20%. (TR 284-285). They decided Complainant should stay in his position.
(TR 285). In 1994 Respondent wanted a 20% reduction of the work force. As a result, they
wanted management to list the lower 40% of each group as well as those positions to be
abolished. (TR 287). It was decided that ISEG would be cut down from 9 positions to 5
positions. (TR 289). The 5 remaining positions had to be filled by engineers. (TR 289). At a
Sunday meeting of senior management, Jim Spadafore was informed of the cuts. (TR 289).
The review board voted 6 to 1 for moving Complainant into
transition. (TR 291). Before the vote, they had forms on each employee that provided
[Page 15]
information on the manager's evaluation, resume of experience, and a feedback form of the
employee. (See RX-6 for the packet of information on Complainant that was used by the
review board, and RX-7 for the packet of information on Darshan Suri). Along with verbal
comments made by board members. (TR 292).
Pat O'Brien was also before the review board. (TR 295).
Complainant had been ranked 6th out of eight. (RX-6). Mr. Suri had been ranked 7th out of
eight. (RX-7).
Mr. Terry thought the Complainant was competent in terms of his
engineering capability but was lacking in terms of communication.4 (TR 297). He had met with Mr. Suri about
his performance and ranking within the group. (TR 298). Mr. Suri pointed out his
accomplishments. Mr. Terry did not give Suri any feedback at the meeting. (TR 299).
There was no discussion of rotation when voting on names in the
review board. (TR 301). The review board ranked Mr. Suri and Complainant differently than the
branch manager. (TR 301). It was fairly common for the review board to disagree with the
branch manager because the branch manager did not have a feeling for the types of capability
that were available elsewhere in the plant. (TR 302).
Testimony of Colleen Ware
She did not recall in particular any discussion about Complainant
or Suri. (TR 327-328).
DISCUSSION AND FINDINGS
The initial threshold in proving his case is easily met by the
Complainant. His position as a member of the ISEG was required by the licensing basis that
allowed Niagara Mohawk to operate Unit No. 2. This unit was created solely for the purpose of
discovering and discussing potential safety problems. The name of the group itself recognizes its
independence and purpose. To take adverse action against a member of the group for performing
his job is the prototypical action protected by the statute. Such action would be interference with
the basis on which the Respondent's license was granted.
There is no dispute that the Respondent was aware of the
Complainant's safety complaints. In fact, the Respondent had a procedure for dealing with these
complaints. The PR and procedure recognize the importance of safety issues raised by members
of the ISEG. The history of the Respondent's action taken in response to the Complainant's PR
on the RHR system in 1993 are well documented and verified by all witnesses.
That the Respondent took adverse action against the Complainant
is also not in dispute. He was terminated by the Respondent in 1994.
[Page 16]
The Complainant's explanation of why he was terminated supports
his contention that his persistence in pursuing his safety complaints was the reason for the
adverse action. The PR filed in 1991 is by itself proof of such action. The Complainant's
continued pursuit of this safety problem was supported by his immediate supervisor Jim
Spadafore.
The Complainant relates in detail a discussion he had with Mr.
Abbott as a result of his persistence. This confrontation in which the Complainant was
threatened with termination if he did not drop the complaint is not denied by the Respondent.
Mr. Abbott merely stated he does not recall any such confrontation; this cannot be considered a
denial. The action taken against the Respondent starting after he again raised essentially the
same issue in 1994 indicates a direct link between the warning and the termination action.
These actions constitute proof of a prima facie case by the
Complainant. The burden therefore shifts to the Respondent.
The Respondent's counter argument is that the termination was
motivated by a nondiscriminating action. In support of this the Respondent stated that there was
a general downsizing called rightsizing that took place in 1993-1994 in an effort to streamline the
utility and make it competitive with others in the power business.
The fact that a general downsizing took place in the years 1993-1994 is
not in dispute. According to the published criteria the targeted group consists of
employees whose performance evaluations were in the lower 40%. In 1993-1994 the goal was to
reduce the number of nuclear engineers. If an employee was not in the lower 40% he was not in
danger of termination.
The evidence establishes that the Complainant was repeatedly told
that he was not in the targeted group. Any time he asked any of his superiors he was told he was
not in jeopardy. No one ever told him he was in this group.
The Respondent counters with several arguments. They say that
the Complainant was in the lower 40% and was terminated strictly in accordance with the stated
criteria. A second not wholly consistent position is that there were other nonpublished criteria
that justified the firing of the Complainant.
The first of these arguments is based on performance evaluation
that shows the Complainant in the lower 40%. These evaluations were prepared during the last
stage of the downsizing. There is no indication that they were ever communicated to the
Complainant. They also include different handwriting. Most importantly they are totally
inconsistent with the verbal assurances given to the Complainant.
The document in question is RX6. A close look shows that there is
no indication that this document was communicated to the Complainant or to his immediate
[Page 17]
supervisor. It includes the statement that the position is not being right sized.
The record is consistent in showing that the Complainant was told
he was not in the lower 40% of the rankings. (TR 61, 62, 126). The question remaining is
whether there is any other legitimate reason for terminating the Complainant.
The Complainant received a letter from Mr. Sylvia dated March
15, 1994. (CX 11). Mr. Sylvia confirmed that the Complainant was not in the lower 40%.
He stated the termination was due to the Complainant being included in an ISEG rotation.
It noted that the decision to rotate employees was made after the downsizing was in progress.
The Complainant received another explanation from Kathy Mills, a
member of the Respondent's Human Resources Department. This letter said the Employee was
being terminated because his position has been abolished.
Ultimately the question in this case is one of credibility. The
Complainant has shown that he raised important safety issues with which the Respondent
disagreed. As a result he was threatened with loss of his position. The Respondent doesn't deny
this, but merely states he can't recall the conversation. The Complainant has shown that he was
repeatedly assured he was not in the group eligible for termination. The testimony of all
witnesses confirms this position.
The Respondent, on the other hand, has not shown why the
Complainant was terminated. They have suggested several reasons, none of which is supported
by the evidence. The record shows there was no rotation plan for ISEG engineers. There is also
no evidence that the Complainant's job was abolished. The only performance evaluation
showing the Complainant is in the lower 40% for 1994 is of no value because of its lack of
consistency with other evidence.
Based on the above the Complainant has proved his case and is entitled to
damages.
Damages
There is insufficient information in the record to assess complete
damages. The parties are therefore given until April 15, 1996 to submit detailed statements of
damages, including information about the value of all fringe benefits, separation payments and
subsequent employment. After receipt of this information a Final Order will be issued by May
15, 1996.
GERALD M. TIERNEY
Administrative Law Judge
GMT/ir
[ENDNOTES]
1 The following abbreviations are used
when citing to the record: CX- Complainant's exhibits; RX- Respondent's exhibits; and TR-
Transcript of the hearing.
2 A problem report
("PR") was a standard deficiency reporting system for both units. (TR 24).
3 It was the Complainant's opinion
that a safety evaluation needed to be conducted in response to the PR. In addressing the PR, it
would not have been necessary to make any physical change in the facility or day-to-day
operation of the station. (TR 107-108).
4 In RX-7, Mr. Suri was
described as quick to criticize, getting facts wrong, and verbal skills not always observed. (TR
320).