U.S. Nuclear Regulatory Commission
Operations Center
Event Reports For
03/01/2002 - 03/04/2002
** EVENT NUMBERS **
38518 38602 38611 38634 38741 38742 38743 38744 38745 38746 38747
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 38518 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: POINT BEACH REGION: 3 |NOTIFICATION DATE: 11/26/2001|
| UNIT: [1] [2] [] STATE: WI |NOTIFICATION TIME: 13:37[EST]|
| RXTYPE: [1] W-2-LP,[2] W-2-LP |EVENT DATE: 11/26/2001|
+------------------------------------------------+EVENT TIME: 12:32[CST]|
| NRC NOTIFIED BY: ROBERT ADAMS |LAST UPDATE DATE: 03/01/2002|
| HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |BRUCE JORGENSEN R3 |
|10 CFR SECTION: | |
|NONR OTHER UNSPEC REQMNT | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE
|
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
|2 N Y 100 Power Operation |100 Power Operation |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| ERDS INOPERABLE DUE TO PLANNED OUTAGE OF THE PLANT PROCESS COMPUTER
SYSTEM |
| (PPCS) |
| |
| AT 1232 CT, the Point Beach Nuclear Plant ERDS became inoperable as a result |
| of modifications to change out the plant process computer system (PPCS). |
| This is a planned evolution. ERDS will remain inoperable until |
| approximately, December 18, 2001. |
| |
| This information was verbally provided to a representative of NRR during the |
| week of 10/15/2001. The senior resident inspector has also been briefed on |
| the modifications and schedule. NMC to NRC letter (NRC 01-0080) dated |
| 11/21/2001 stated we would be submitting this Non-Emergency report. |
| |
| ***** UPDATE FROM RICK ROBBINS TO LEIGH TROCINE AT 2006 EST ON 11/27/01 |
| ***** |
| |
| The following additional information is a portion of a facsimile received |
| from the licensee: |
| |
| "As part of the PPCS modification, several inputs to the SPDS monitor were |
| also made unavailable. Any out-of-service indications on the SPDS can be |
| obtained by control room control board indications." |
| |
| The licensee notified the NRC resident inspector. The NRC operations center |
| notified the R3DO (Bruce Jorgensen). |
| |
| * * * UPDATE 1259EST ON 12/22/01 FROM RYAN RODE TO S. SANDIN * * * |
| |
| The licensee provided the following information as an update: |
| |
| "On 11/26/01 at 12:32, the PBNP ERDS and SPDS were declared out of service |
| for the PPCS upgrade project. EN #38518 indicated to the NRC that the |
| systems would remain unavailable until approximately December 18, 2001. Due |
| to reliability issues with the newly installed PPCS, that expected date has |
| been delayed to approximately January 3, 2002." |
| |
| The licensee informed the NRC Resident Inspector. Notified R3DO(Phillips). |
| |
| * * * UPDATE ON 01/03/02 @1430 BY MEYER TO GOULD * * * |
| |
| During the installation of the new PPCS, issues were identified which need |
| to be resolved to allow SPDS and ERDS to be placed back in service fully. |
| Currently, the new PPCS is only partially operable. Work is continuing on |
| the new PPCS to allow full operability. The current estimate for return to |
| service of SPDS and ERDS is 01/19/02. This date may need to be extended |
| again due to parts availability. |
| |
| The NRC Resident Inspector was notified. |
| |
| Notified Reg 3 RDO(Shear) |
| |
| * * * UPDATE ON 1/17/02 @ 1855 BY HARRSCH TO GOULD * * * |
| |
| Update to 1/3/02 update (see below). Work continues on the Plant Process |
| Computer System (PPCS) to allow full operability. The Safety Parameter |
| Display System (SPDS) is still out of service, however the Emergency |
| Response Data System (ERDS) is now available. As mentioned in the 1/3/02 |
| update, parts availability has been a problem and the date for returning |
| SPDS to service is now estimated to be 2/16/02. |
| |
| The NRC Resident Inspector was notified. |
| |
| Reg 3 RDO(Vegel) was informed |
| |
| ***UPDATE ON 2/15/02 @ 1323 EST BY ADAMS TO NORRIS*** |
| |
| Update to 1/17/02 update. Work continues on the Plant Process Computer |
| System (PPCS) to allow full operability. The Safety Parameter Display System |
| (SPDS) is still out of service. Due to parts availabilty, the date for |
| returning SPDS to service is now estimated to be 3/09/02. |
| |
| The NRC Resident Inspector was notified. |
| |
| Reg 3 RDO(Vegel) was informed. |
| |
| ***UPDATE ON 3/1/02 @ 1145 EST BY MILLEN TO NORRIS*** |
| |
| Update to 1/17/02 event notification. As part of the upgade to the Plant |
| Process Comuter System (PPCS), the Safety Parameter Display System (SPDS) |
| has been accepted for use and is considered fully operational. |
| |
| The NRC Resident Inspector was notified. |
| |
| Reg 3 RDO (Lipa) was informed. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 38602 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: CRYSTAL RIVER REGION: 2 |NOTIFICATION DATE: 01/01/2002|
| UNIT: [3] [] [] STATE: FL |NOTIFICATION TIME: 10:08[EST]|
| RXTYPE: [3] B&W-L-LP |EVENT DATE: 01/01/2002|
+------------------------------------------------+EVENT TIME: 09:19[EST]|
| NRC NOTIFIED BY: BILL BANDHAUER |LAST UPDATE DATE: 03/01/2002|
| HQ OPS OFFICER: FANGIE JONES +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |ANNE BOLAND R2 |
|10 CFR SECTION: | |
|APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE
|
+-----+----------+-------+--------+-----------------+--------+-----------------+
|3 N Y 100 Power Operation |100 Power Operation |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| OFFSITE NOTIFICATION DUE RESCUED SEA TURTLE |
| |
| EN #37902 started the biennial report period. |
| |
| On January 1, 2002 at 0919, a rescued sea turtle was identified as a green |
| sea turtle. This is the 62nd rescue of a live sea turtle at Crystal River |
| Unit 3 (CR-3) in this biennial period. Notification to the National Marine |
| Fisheries Service and the Florida Fish and Wildlife Conservation Commission. |
| |
| |
| The licensee intends to notify the NRC Resident Inspector. |
| |
| * * * UPDATE ON 1/05/02 @ 1002 BY RAWLS TO GOULD * * * |
| |
| On January 5, 2002, at 0720, a rescued sea turtle was identified as a |
| Loggerhead Sea Turtle. This is the 63rd rescue of a live sea turtle at |
| Crystal River Unit 3 (CR3) in this biennial period. This is reportable as a |
| 4-hour report under 10 CFR 50.72(b)(2)(xi) as this event is related to the |
| protection of the environment for which a notification to other government |
| agencies (National Marine Fisheries Service and Florida Fish and Wildlife |
| Conservation Commission) has been or will be made. |
| |
| The NRC Resident Inspector was notified. |
| |
| Reg 2 RDO (Decker) was notified. |
| |
| * * * UPDATE ON 01/09/02 @ 1107 EST BY ANDY BARNES TAKEN BY MACKINNON * * * |
| |
| On January 9, 2002, at 0838, a rescued sea turtle was identified as a Kemp's |
| Ridley Sea Turtle. This is the 64th rescue of a live turtle at Crystal River |
| Unit 3 (CR-3) in this biennial period. This is reportable as a 4-hour 10 CFR |
| 50.72 (b)(2)(xi) as this event is related to the protection of the |
| environment for which a notification to other government agencies (National |
| Marine Fisheries Service and Florida Fish and Wildlife Conservation |
| Commission) has been or will be made. |
| |
| The NRC Resident Inspector was notified. |
| |
| Reg 2 (Brian Bonser) was notified. |
| |
| * * * UPDATE ON 02/17/02 at 0940 EST BY RICKY RAWLS TO FANGIE JONES * * * |
| |
| "On February 17, 2002 at 0820, a rescued injured sea turtle was identified |
| as a Kemp's Ridley Sea Turtle. The injury will require transportation to |
| Clearwater Marine Science Center or Florida Fish and Wildlife Conservation |
| Refuge. The Injury appears to be from a boat propeller. This is the 65th |
| rescue of a live sea turtle at Crystal River Unit 3 (CR-3) in this biennial |
| period. This is Reportable as a 4-Hour Report under 10 CFR 50.72(b) (2) (xi) |
| as this event is related to the protection of the environment for which a |
| notification to other government agencies (National Marine Fisheries Service |
| and Florida Fish and Wildlife Conservation Commission) has been or will be |
| made. This Is an update to event 38602." |
| |
| The NRC Resident Inspector will be notified. R2DO (Stephen Cahill) has been |
| notified. |
| |
| * * * UPDATE ON 03/01/02 AT 1122 EST BY RICKY RAWLS TO GERRY WAIG * * * |
| |
| "On March 1, 2002 at 0952, a healthy rescued sea turtle was identified as a |
| Green Sea Turtle. This is the 66th rescue of a live sea turtle at Crystal |
| River Unit 3 (CR-3) in this biennial period. This is Reportable as a 4-Hour |
| Report under 10 CFR 50.72 (b) (2) (xi) as this event is related to the |
| protection of the environment for which a notification to other government |
| agencies (National Marine Fisheries Service and Florida Fish and Wildlife |
| Conservation Commission) has been or will be made. This is an update to |
| event 38602." |
| |
| The NRC Resident Inspector was notified. R2DO (Julian) was notified. |
+------------------------------------------------------------------------------+
!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!!
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 38611 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: HOPE CREEK REGION: 1 |NOTIFICATION DATE: 01/06/2002|
| UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 21:42[EST]|
| RXTYPE: [1] GE-4 |EVENT DATE: 01/06/2002|
+------------------------------------------------+EVENT TIME: 14:10[EST]|
| NRC NOTIFIED BY: PARKER |LAST UPDATE DATE: 03/01/2002|
| HQ OPS OFFICER: JOHN MacKINNON +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |MOHAMED SHANBAKY R1 |
|10 CFR SECTION: | |
|AIND 50.72(b)(3)(v)(D) ACCIDENT MITIGATION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE
|
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| HIGH PRESSURE COOLANT INJECTION (HPCI) SYSTEM DECLARED INOPERABLE
|
| |
| During the performance of the quarterly valve surveillance test for the HPCI |
| system, a testable check valve, 1FD-V032, related to the HPCI Barometric |
| Condenser Discharge Line, failed. This failure rendered the HPCI system |
| inoperable at 1410 EST on 01/06/02. The licensee entered an active 14 day |
| Limiting Condition of Operation that expires on 01/20/02 at 1410 EST. All |
| other safety systems are operable. Current plans to return plant to normal |
| configuration include the development of corrective maintenance work |
| package. |
| |
| The NRC Resident Inspector will be notified of this event by the licensee. |
| |
| ***3/1/02 0952 Event was retracted by Licensee; Jim Priest to Mike |
| Norris.*** |
| |
| "PSEG Nuclear retracts the event notification made on 1/6/02 (event number |
| 38611). |
| |
| "Barometric condenser condensate pump discharge check valve 1 FD-V032 was |
| opened and inspected. The valve internals were cleaned and the valve was |
| reassembled and retested satisfactorily. |
| |
| "Subsequent evaluation determined that failure of 1 FD-V032 to close would |
| not have prevented the HPCI system from performing its safety function. |
| Reverse flow through 1 FD-V032 would not degrade the flow that HPCI supplies |
| the reactor vessel during a postulated accident. |
| |
| "Since the HPCI system remained capable of performing its safety function, |
| this event is not reportable. |
| |
| "The NRC Resident Inspector has been notified of this event by the |
| licensee." |
| |
| Notified R1DO (Linville) |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 38634 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 01/17/2002|
| UNIT: [1] [2] [] STATE: FL |NOTIFICATION TIME: 13:07[EST]|
| RXTYPE: [1] CE,[2] CE |EVENT DATE: 01/17/2002|
+------------------------------------------------+EVENT TIME: 11:45[EST]|
| NRC NOTIFIED BY: KELLY KORTH |LAST UPDATE DATE: 03/02/2002|
| HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |ROBERT HAAG R2 |
|10 CFR SECTION: | |
|APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE
|
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
|2 N Y 100 Power Operation |100 Power Operation |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| OFFSITE NOTIFICATION INVOLVING RECOVERED SEA TURTLE FROM INTAKE CANAL
|
| |
| At approximately 1130 EST on 01/17/02, a green sea turtle was retrieved from |
| the intake canal and a determination was made that it was in need of |
| rehabilitation. As required by the Plant's Sea Turtle Permit, the Florida |
| Fish and Wildlife Conservation Commission (FFWCC) was notified at 1145 EST. |
| |
| The licensee notified the NRC Resident Inspector. |
| |
| See EN #38513 for 2001 occurrences. |
| |
| * * * UPDATE ON 1/28/02 @ 1243 BY KORTH TO GOULD * * * |
| |
| At approximately 1115 on 1/28/02 a loggerhead turtle was retrieved from the |
| plant's intake canal. The turtle was determined to be in need of |
| rehabilitation. Per the licensee's turtle permit, the Florida Fish and |
| Wildlife Conservation Commission (FWCC) was notified at 1125. |
| |
| The NRC Resident Inspector was notified. Notified Reg 2 RDO (Ninh) |
| |
| |
| * * * UPDATE ON 2/6/02 @ 0853 BY MERRILL TO GOULD * * * |
| |
| At approximately 0745 on 2/6/02 an injured green sea turtle was rescued from |
| the plant's intake canal. The turtle was alive, but in need of |
| rehabilitation. The turtle will be transported to a facility in Clearwater |
| for treatment. The Florida Department of Environmental Protection has been |
| notified of the event. |
| |
| The NRC Resident Inspector was notified. |
| |
| Notified Reg 2 RDO(Fredrickson) |
| |
| * * * UPDATE 1025 3/2/2002 BY R. DIEHL TAKEN BY R. STRANSKY * * * |
| |
| "At approximately 0830 3/2/02 a Loggerhead turtle was retrieved from the |
| plant's intake canal. The turtle was determined to be in need of |
| rehabilitation. Per the plant's turtle permit, the Florida Fish and Wildlife |
| Conservation Commission (FWCC) was notified at 0845." |
| |
| The NRC resident inspector has been informed of this report. HOO notified |
| R2DO (Julian). |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 38741 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: LIMERICK REGION: 1 |NOTIFICATION DATE: 03/01/2002|
| UNIT: [1] [2] [] STATE: PA |NOTIFICATION TIME: 02:29[EST]|
| RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 03/01/2002|
+------------------------------------------------+EVENT TIME: 02:16[EST]|
| NRC NOTIFIED BY: PHILIP CHASE |LAST UPDATE DATE: 03/01/2002|
| HQ OPS OFFICER: STEVE SANDIN +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |JAMES LINVILLE R1 |
|10 CFR SECTION: | |
|DDDD 73.71 UNSPECIFIED PARAGRAPH | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE
|
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 87 Power Operation |87 Power Operation |
|2 N Y 100 Power Operation |100 Power Operation |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| SECURITY REPORT |
| |
| Unescorted access granted inappropriately to contract employee. Immediate |
| compensatory measures taken upon discovery. The licensee will inform the |
| NRC resident inspector. Contact the Headquarters Operations Officer for |
| additional details. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|General Information or Other |Event Number: 38742 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG: TEXAS DEPARTMENT OF HEALTH |NOTIFICATION DATE: 03/01/2002|
|LICENSEE: PROTECHNICS |NOTIFICATION TIME: 08:52[EST]|
| CITY: HOUSTON REGION: 4 |EVENT DATE: 02/14/2002|
| COUNTY: HARRIS STATE: TX |EVENT TIME: [CST]|
|LICENSE#: LO3835 AGREEMENT: Y |LAST UPDATE DATE: 03/01/2002|
| DOCKET: |+----------------------------+
| |PERSON ORGANIZATION |
| |DAVID GRAVES R4 |
| |FRED BROWN NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: JAMES H. OGDEN JR. | |
| HQ OPS OFFICER: MIKE NORRIS | |
+------------------------------------------------+ |
|EMERGENCY CLASS: NON EMERGENCY | |
|10 CFR SECTION: | |
|NAGR AGREEMENT STATE | |
| | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| AGREEMENT STATE REPORT INVOLVING A STUCK LOGGING WELL SOURCE |
| |
| "Well logging tool became stuck at 17,125 feet, top of tool is 17,106 feet. |
| Attempted fishing on 3 consecutive days, unsuccessful. Pumped 466 feet of |
| red cement to secure source on February 14, 2002, to plug well. Top of plug |
| is 16,640 feet. Permanent identification plaque is under construction for |
| emplacement on the wellhead. Abandoned at Frank Bell #1 RE, Leon County, |
| Texas, AP# 42-289-30432. Source abandoned IAW Texas Regulations. |
| |
| "Isotope Products Laboratory, sealed logging source (Capsule Type), Model # |
| HEG-241, Serial # NN-082, 250 microcuries Am-241. Last leak tested 09/07/01 |
| (No leakage). Manufactured September 25, 1998, pressure tested to 25,000 |
| psi." |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 38743 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: WATTS BAR REGION: 2 |NOTIFICATION DATE: 03/01/2002|
| UNIT: [1] [] [] STATE: TN |NOTIFICATION TIME: 10:20[EST]|
| RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 03/01/2002|
+------------------------------------------------+EVENT TIME: 02:59[EST]|
| NRC NOTIFIED BY: R. Kimbrough |LAST UPDATE DATE: 03/01/2002|
| HQ OPS OFFICER: GERRY WAIG +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |CAUDLE JULIAN R2 |
|10 CFR SECTION: | |
|AINB 50.72(b)(3)(v)(B) POT RHR INOP | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE
|
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N N 0 Refueling |0 Refueling |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| UNIT EXPERIENCED MOMENTARY LOSS OF RHR COOLING |
| |
| "At approximately 0259 on March 1, 2002, with the Watts Bar Unit 1 reactor |
| in Mode 6 with RCS temperature at approximately 100 degrees, during a |
| refueling outage, operators isolated the common flowpath to the residual |
| heat removal (RHR) pumps on two occasions over a 2 minute span. At the time |
| of the event, operators were performing full flow testing of ECCS lines in |
| conjunction with reactor cavity fill for refueling activities. |
| |
| The circumstances of the event are currently under investigation by the Site |
| staff." |
| |
| No observable RCS heatup occurred during the period that RHR was isolated. |
| |
| The NRC resident inspector was notified. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|General Information or Other |Event Number: 38744 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG: LOUISIANA RADIATION PROTECTION DIV |NOTIFICATION DATE: 03/01/2002|
|LICENSEE: METCO SULPHUR |NOTIFICATION TIME: 15:05[EST]|
| CITY: REGION: 4 |EVENT DATE: 02/22/2002|
| COUNTY: STATE: LA |EVENT TIME: 18:30[CST]|
|LICENSE#: LA-8043-L01 AGREEMENT: Y |LAST UPDATE DATE: 03/01/2002|
| DOCKET: |+----------------------------+
| |PERSON ORGANIZATION |
| |DAVID GRAVES R4 |
| |FRED BROWN NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: SCOTT BLACKWELL | |
| HQ OPS OFFICER: GERRY WAIG | |
+------------------------------------------------+ |
|EMERGENCY CLASS: NON EMERGENCY | |
|10 CFR SECTION: | |
|NAGR AGREEMENT STATE | |
| | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| AGREEMENT STATE REPORT - LOCK MALFUNCTION ON CAMERA |
| |
| "On Friday February 22, 2002, a radiographer from METCO discovered that the |
| lock on the Amersham 660 radiography camera with 60 curies of Ir-192 would |
| not release to allow an exposure. The Environmental Manager from LA Pigment |
| believed the auto-lock on the exposure device failed. The RSO at METCO |
| responded within 30 minutes. The RSO stated that he cleaned the lock with |
| WD-40 and the lock functioned after that. The RSO believes the lock was just |
| dirty." |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 38745 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: HARRIS REGION: 2 |NOTIFICATION DATE: 03/01/2002|
| UNIT: [1] [] [] STATE: NC |NOTIFICATION TIME: 18:14[EST]|
| RXTYPE: [1] W-3-LP |EVENT DATE: 03/01/2002|
+------------------------------------------------+EVENT TIME: [EST]|
| NRC NOTIFIED BY: MARK ELLINGTON |LAST UPDATE DATE: 03/01/2002|
| HQ OPS OFFICER: FANGIE JONES +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |CAUDLE JULIAN R2 |
|10 CFR SECTION: | |
|AUNA 50.72(b)(3)(ii)(B) UNANALYZED CONDITION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE
|
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| UNANALYZED CONDITION DUE TO FIRE BARRIERS NOT INSTALLED PER DESIGN
|
| |
| "On March 1, 2002, Harris Nuclear Plant personnel determined that an |
| unanalyzed condition existed due to a required three-hour fire barrier not |
| installed per design. The applicable fire barrier was designed to provide |
| required separation between redundant train cables supplying A-SA Emergency |
| Diesel Generator and B-SB Emergency Diesel Generator. Harris Nuclear Plant |
| has initiated a continuous fire watch as a compensatory measure until the |
| affected barrier could be restored to the design configuration. This issue |
| is being reported in accordance with 10 CFR 50.72 as an unanalyzed |
| condition." |
| |
| The licensee notified the NRC Resident Inspector. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 38746 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SALEM REGION: 1 |NOTIFICATION DATE: 03/03/2002|
| UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 04:25[EST]|
| RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 03/03/2002|
+------------------------------------------------+EVENT TIME: 02:18[EST]|
| NRC NOTIFIED BY: VAN FORD |LAST UPDATE DATE: 03/03/2002|
| HQ OPS OFFICER: BOB STRANSKY +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |JAMES LINVILLE R1 |
|10 CFR SECTION: | |
|APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE
|
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |45 Power Operation |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| OFFSITE NOTIFICATION DUE TO OIL SPILL INTO DELAWARE RIVER |
| |
| "On March 3, 2002 at 0218 a cooling line to 12B circulating water pump upper |
| motor bearing ruptured inside the upper oil reservoir. Oil was displaced |
| from the oil reservoir and approximately 50 gallons of oil entered the |
| Delaware River. 12B circulating water pump was removed from service and the |
| leak was terminated. Cleanup efforts by onsite personnel are in progress. A |
| 15 minute report was made to the New Jersey Department of Environmental |
| Protection. A two hour report was made to the National Response Center in |
| accordance with the site spill plan. |
| |
| Salem Unit 1 was initially at 100% power with 13B circulating water pump out |
| of service for scheduled maintenance. Power reduction is currently in |
| progress in response to the loss of 12B circulating water pump with a target |
| power level of 40%." |
| |
| The NRC resident inspector has been informed of this notification by the |
| licensee. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 38747 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SUSQUEHANNA REGION: 1 |NOTIFICATION DATE: 03/03/2002|
| UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 06:04[EST]|
| RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 03/03/2002|
+------------------------------------------------+EVENT TIME: 03:00[EST]|
| NRC NOTIFIED BY: GORDON ROBINSON |LAST UPDATE DATE: 03/03/2002|
| HQ OPS OFFICER: BOB STRANSKY +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |JAMES LINVILLE R1 |
|10 CFR SECTION: | |
|ADEG 50.72(b)(3)(ii)(A) DEGRADED CONDITION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE
|
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N N 0 Cold Shutdown |0 Cold Shutdown |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| MSIV LEAKAGE EXCEEDS ALLOWABLE LIMIT |
| |
| "Leak Rate Testing on Unit 1 Main Steam Isolation Valves has identified that |
| the total minimum pathway leak rate exceeds the required limit of 300 scfh. |
| The MSIV pathway combined leak rate was 1051 scfh. The identified degraded |
| condition is reportable as a condition of the nuclear power plant, including |
| its principal safety barriers being seriously degraded per |
| 10CFR50.72(b)(3)(ii)." |
| |
| The NRC resident inspector will be informed of this notification by the |
| licensee. |
+------------------------------------------------------------------------------+