U.S. Nuclear Regulatory Commission
Operations Center
Event Reports For
04/13/1999 - 04/14/1999
** EVENT NUMBERS **
35512 35579 35586 35587 35588 35589 35590 35591
!!!!!!!!! THIS EVENT HAS BEEN RETRACTED. THIS EVENT HAS BEEN RETRACTED !!!!!!!
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 35512 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: COMANCHE PEAK REGION: 4 |NOTIFICATION DATE: 03/25/1999|
| UNIT: [1] [2] [] STATE: TX |NOTIFICATION TIME: 17:37[EST]|
| RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 03/25/1999|
+------------------------------------------------+EVENT TIME: 16:04[CST]|
| NRC NOTIFIED BY: TOM BEAUDIN |LAST UPDATE DATE: 04/13/1999|
| HQ OPS OFFICER: FANGIE JONES +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |CHARLES CAIN R4 |
|10 CFR SECTION: | |
|DDDD 73.71 UNSPECIFIED PARAGRAPH | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
|2 N N 0 Refueling |0 Refueling |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| PHYSICAL SECURITY REPORT |
| |
| Unescorted access granted inappropriately to contract employee. Immediate |
| compensatory measures taken upon discovery. |
| |
| The licensee notified the NRC Resident Inspector. |
| |
| Refer to the HOO Log for additional details. |
| |
| *** UPDATE ON 04/12/99 @ 1418 BY HARRIS TO GOULD *** RETRACTION |
| |
| THE LICENSEE IS RETRACTING THIS EVENT. REFER TO HOO LOG FOR ADDITIONAL |
| INFORMATION. |
| |
| THE RESIDENT INSPECTOR WILL BE NOTIFIED. |
| |
| THE REG 4 RDO(SMITH) WAS NOTIFIED. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 35579 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: MONTICELLO REGION: 3 |NOTIFICATION DATE: 04/12/1999|
| UNIT: [1] [] [] STATE: MN |NOTIFICATION TIME: 15:10[EDT]|
| RXTYPE: [1] GE-3 |EVENT DATE: 04/12/1999|
+------------------------------------------------+EVENT TIME: 14:00[CDT]|
| NRC NOTIFIED BY: PEDERSON |LAST UPDATE DATE: 04/13/1999|
| HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |JOHN JACOBSON R3 |
|10 CFR SECTION: | |
|AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | |
|NLCO TECH SPEC LCO A/S | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| PLANT DECLARED HPCI INOPERABLE DUE TO THE LOSS OF THE EMERGENCY SERVICE |
| WATER TO ONE OF TWO VENTILATION UNITS. |
| |
| THE EMERGENCY SERVICE WATER WAS LOST AS A RESULT OF THE FAILURE OF #13 |
| EMERGENCY SERVICE WATER PUMP TO START, WHICH PUT HPCI OUT OF SERVICE AND |
| THE PLANT IN A 24 HR TO SHUTDOWN LCO ACTION STATEMENT. WHEN THEY ATTEMPTED |
| TO START #13 EMERGENCY SERVICE WATER PUMP, THE MOTOR WOULD HUM BUT THE |
| IMPELLER WOULD NOT TURN AND THAT RESULTED IN THE TRIP OF THE PUMP BREAKER. |
| THEY MANUALLY TRIED TO TURN THE IMPELLER , WHICH SEEMED STUCK INITIALLY, BUT |
| THEY FINALLY GOT IT TO TURN FREELY. THERE MAY HAVE BEEN SOME TYPE OF |
| DEBRIS THAT WAS CAUSING THE IMPELLER NOT TO TURN. CURRENTLY THEY ARE |
| PERFORMING OPERABILITY CHECKS ON THE PUMP SO THAT THE LCO CAN BE EXITED. |
| DURING THIS EVENT THE NORMAL SERVICE WATER WAS AVAILABLE. |
| |
| THE RESIDENT INSPECTOR WAS NOTIFIED. |
| |
| *** UPDATE ON 4/12/99 @ 1618 BY PEDERSON TO GOULD *** |
| |
| HPCI OPERABLE AFTER RESTORATION OF THE #13 EMERGENCY SERVICE WATER SYSTEM. |
| LCO EXITED AT 1507 CDT. |
| |
| THE RESIDENT INSPECTOR WAS NOTIFIED. |
| |
| REG 3 RDO(JACOBSON) WAS INFORMED. |
| |
| * * * UPDATE AT 1007 EDT ON 4/13/99 BY BRUCE MACKISSOCK TO FANGIE JONES * * |
| * |
| |
| The time of the event was reported as 1400 CDT, it should be 0755 CDT. |
| Notified R3DO (John Jacobson). |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 35586 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: BEAVER VALLEY REGION: 1 |NOTIFICATION DATE: 04/13/1999|
| UNIT: [1] [] [] STATE: PA |NOTIFICATION TIME: 05:55[EDT]|
| RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 04/13/1999|
+------------------------------------------------+EVENT TIME: 04:27[EDT]|
| NRC NOTIFIED BY: CHRIS HYNES |LAST UPDATE DATE: 04/13/1999|
| HQ OPS OFFICER: FANGIE JONES +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |DAN HOLODY R1 |
|10 CFR SECTION: | |
|ARPS 50.72(b)(2)(ii) RPS ACTUATION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 M/R N 0 Hot Standby |0 Hot Standby |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| MANUAL REACTOR TRIP DUE TO ROD CONTROL URGENT FAILURE ALARM |
| |
| During a planned plant shutdown, with the reactor already subcritical, |
| control bank 'A' group 2 did not move as rods were being inserted. As a |
| result, the rod control system received an "Urgent Alarm" which inhibited |
| manual control rod motion. The licensee performed a manual trip and all |
| rods fully inserted. The problem is being investigated. |
| |
| Heat removal was and is by steam dump to the main condenser with feedwater |
| from the main feedwater system. |
| |
| The licensee notified the NRC Resident Inspector. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 35587 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: NORTH ANNA REGION: 2 |NOTIFICATION DATE: 04/13/1999|
| UNIT: [1] [] [] STATE: VA |NOTIFICATION TIME: 13:05[EDT]|
| RXTYPE: [1] W-3-LP,[2] W-3-LP |EVENT DATE: 04/13/1999|
+------------------------------------------------+EVENT TIME: 10:25[EDT]|
| NRC NOTIFIED BY: CROSSMAN |LAST UPDATE DATE: 04/13/1999|
| HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |PIERCE SKINNER R2 |
|10 CFR SECTION: | |
|AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | |
|NLCO TECH SPEC LCO A/S | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| THE CONTROL ROOM EMERGENCY VENTILATION FAN SUCTION SUPPLY DAMPER SWITCH |
| FOUND IN THE INCORRECT POSITION. |
| |
| THE CONTROL ROOM EMERGENCY FAN, "1-HV-F-42", SUCTION SUPPLY DAMPER SWITCH |
| WAS FOUND IN THE "NORMAL MODE" POSITION INSTEAD OF THE "LOCKOUT" POSITION. |
| THE SWITCH HAS TO BE IN THE "LOCKOUT" POSITION TO MAINTAIN THE CONTROL ROOM |
| PRESSURE ENVELOPE IN THE RECIRCULATION MODE DURING THE INITIAL STAGES OF A |
| FUEL HANDLING ACCIDENT OR SAFETY INJECTION. BY THE SWITCH BEING IN THE |
| INCORRECT POSITION(NORMAL MODE) IT WOULD HAVE AFFECTED THE ABILITY OF THE |
| FAN TO PERFORM ITS ACCIDENT FUNCTION. THE PLANT ENTERED A 7 DAY LCO UNDER |
| TS 3.7.7.1 WHICH REQUIRES CORRECTIVE MEASURES TO BE IMPLEMENTED. THE SWITCH |
| WAS PLACED IN THE CORRECT, "LOCKOUT", POSITION AT 10:32 AM. INVESTIGATION |
| ON HOW THE SWITCH GOT INTO THE INCORRECT POSITION IS ONGOING. |
| |
| THE RESIDENT INSPECTOR WAS NOTIFIED. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Other Nuclear Material |Event Number: 35588 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG: SEA WORLD OF OHIO |NOTIFICATION DATE: 04/13/1999|
|LICENSEE: SEA WORLD OF OHIO |NOTIFICATION TIME: 14:21[EDT]|
| CITY: AURORA REGION: 3 |EVENT DATE: 04/12/1999|
| COUNTY: STATE: OH |EVENT TIME: 12:00[EDT]|
|LICENSE#: AGREEMENT: N |LAST UPDATE DATE: 04/13/1999|
| DOCKET: |+----------------------------+
| |PERSON ORGANIZATION |
| |JOHN JACOBSON R3 |
| |FRED COMBS NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: ROBERTS | |
| HQ OPS OFFICER: CHAUNCEY GOULD | |
+------------------------------------------------+ |
|EMERGENCY CLASS: N/A | |
|10 CFR SECTION: | |
|ELOS 39.77(b) THEFT/LOSS OF RAD MAT | |
| | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| SEA WORLD OF OHIO LOCATED IN AURORA, OHIO REPORTED THAT ONE OF THEIR TRITIUM |
| EXIT SIGNS WAS MISSING. |
| |
| A SEARCH FOR THIS SIGN WAS MADE PRIOR TO MAKING THE DETERMINATION THAT IT |
| WAS LOST. THE EXIT SIGN WAS MANUFACTURED BY SELF POWERED LIGHTING INC. OF |
| ELMSFORD, N.Y. |
| THE NAME OF THE SIGN IS OMNIGLO MODEL 700C-12 S/N C-5072 CONTAINING 20 |
| CURIES OF TRITIUM. |
| DATE OF MANUFACTURE WAS 12/88 AND EXPIRATION DATE IS 12/00. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Fuel Cycle Facility |Event Number: 35589 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 04/13/1999|
| RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 14:40[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 04/11/1999|
| 6903 ROCKLEDGE DRIVE |EVENT TIME: 21:45[CDT]|
| BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 04/13/1999|
| CITY: PADUCAH REGION: 3 +-----------------------------+
| COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION |
|LICENSE#: GDP-1 AGREEMENT: Y |JOHN JACOBSON R3 |
| DOCKET: 0707001 |FRED COMBS NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: HALICKS | |
| HQ OPS OFFICER: CHAUNCEY GOULD | |
+------------------------------------------------+ |
|EMERGENCY CLASS: N/A | |
|10 CFR SECTION: | |
|OCBB 76.120(c)(2)(ii) EQUIP DISABLED/FAILS | |
| | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| THE PLANT SHIFT SUPERINTENDENT(PSS) WAS NOTIFIED THAT THERE HAD BEEN A |
| FAILURE OF THE UF6 RELEASE DETECTION SYSTEM IN THE C-333 PROCESS BUILDING |
| UNIT 5 CELL 4. THE FAILURE OCCURRED DURING THE TWICE-PER-SHIFT TSR |
| SURVEILLANCE WHICH REQUIRES "TEST FIRING" OF THE DETECTOR HEADS. THE PSS |
| IMMEDIATELY DECLARED THE SAFETY SYSTEM INOPERABLE AND DIRECTED THE |
| IMPLEMENTATION OF TSR-REQUIRED ACTIONS WHICH INCLUDE PLACING A "SMOKE WATCH" |
| IN THE AFFECTED AREA. IN ADDITION, THE OPERATING PRESSURE OF THE AFFECTED |
| EQUIPMENT WAS REDUCED TO BELOW ATMOSPHERIC PRESSURE WHICH PLACED THE |
| EQUIPMENT IN A MODE IN WHICH THE SAFETY SYSTEM WAS NOT REQUIRED TO BE |
| AVAILABLE AND OPERABLE. THE PSS WAS SUBSEQUENTLY NOTIFIED (AT 0130 ON |
| 4/12/99) THAT THE EQUIPMENT HAD ACTUALLY FAILED DURING THE TEST AT |
| APPROXIMATELY 2145. COMPENSATORY ACTIONS WERE NOT IMPLEMENTED IN A TIMELY |
| MANNER IN ACCORDANCE WITH THE APPLICABLE TSR. THE TSR-REQUIRED ACTIONS WERE |
| REQUIRED TO BE IMPLEMENTED WITHIN 1 HOUR AND WERE IMPLEMENTED APPROXIMATELY |
| 80 MINUTES LATE. |
| |
| THIS EVENT IS BEING SUBMITTED LATE DUE TO A MISINTERPRETATION OF THE EVENT |
| REPORTING CRITERIA. |
| |
| THE RESIDENT INSPECTOR HAS BEEN NOTIFIED. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 35590 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: GINNA REGION: 1 |NOTIFICATION DATE: 04/13/1999|
| UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 17:58[EDT]|
| RXTYPE: [1] W-2-LP |EVENT DATE: 04/13/1999|
+------------------------------------------------+EVENT TIME: 15:25[EDT]|
| NRC NOTIFIED BY: GOMEZ |LAST UPDATE DATE: 04/13/1999|
| HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |DAN HOLODY R1 |
|10 CFR SECTION: | |
|AESF 50.72(b)(2)(ii) ESF ACTUATION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N N 0 Cold Shutdown |0 Cold Shutdown |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| PLANT HAD AUTO START AND LOADING OF THE EMERGENCY DIESEL "B". |
| |
| THE PLANT IS IN MODE 5 FOR A REFUELING OUTAGE AND PERSONNEL WERE PERFORMING |
| A SAFETY INJECTION FUNCTIONAL TEST. THIS TEST REQUIRES THE EMERGENCY DIESEL |
| "B" TO BE PLACED IN LOCKOUT WHILE DEENERGIZING THE SAFEGUARDS BUSES. UPON |
| COMPLETION OF THIS PORTION OF THE TEST, BUS RESTORATION WAS INITIATED. THE |
| RESTORATION STEPS REQUIRE CLOSURE OF BUS 17 (SCREENHOUSE SAFEGUARDS BUS) |
| NORMAL FEEDER BREAKER, BUT IT WOULD NOT CLOSE. RESTORATION CONTINUED WHILE |
| TROUBLESHOOTING THE BUS 17 NORMAL FEEDER BREAKER PROBLEM. WHEN THE STEPS |
| FOR DIESEL GENERATOR "B" WERE PERFORMED, THE DIESEL WAS RESET. UPON RESET, |
| THE DIESEL GENERATOR "B" SAW THE UNDERVOLTAGE ON BUS 17, AUTO STARTED AND |
| LOADED BUS 17 AS DESIGNED. THE DIESEL GENERATOR "B" WAS SECURED AT 1631 AND |
| BUS 17 HAS BEEN REENERGIZED FROM NORMAL POWER SUPPLY. INITIAL |
| INVESTIGATION SHOWED CAUSE OF THE FAILURE OF THE FEEDER BREAKER TO CLOSE WAS |
| DUE TO A BLOWN UNDERVOLTAGE FUSE. |
| |
| THE RESIDENT INSPECTOR WAS NOTIFIED. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 35591 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: COOPER REGION: 4 |NOTIFICATION DATE: 04/14/1999|
| UNIT: [1] [] [] STATE: NE |NOTIFICATION TIME: 04:32[EDT]|
| RXTYPE: [1] GE-4 |EVENT DATE: 04/14/1999|
+------------------------------------------------+EVENT TIME: 01:28[CDT]|
| NRC NOTIFIED BY: FRED SCHIZAS |LAST UPDATE DATE: 04/14/1999|
| HQ OPS OFFICER: DICK JOLLIFFE +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |LINDA SMITH R4 |
|10 CFR SECTION: | |
|AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | |
|NLCO TECH SPEC LCO A/S | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| - RCIC SYSTEM DECLARED INOPERABLE DUE TO FAILED SYSTEM COOLING VALVE DURING |
| A TEST - |
| |
| AT 0128 CDT ON 04/14/99, THE LICENSEE DECLARED THE REACTOR CORE ISOLATION |
| COOLING (RCIC) SYSTEM INOPERABLE DUE TO THE FAILURE OF THE RCIC SYSTEM |
| COOLING VALVE, #RCIC-MO-132. WHEN THE VALVE CONTROL SWITCH WAS PLACED IN |
| THE CLOSE POSITION IN ORDER TO RECORD THE VALVE STROKE TIME DURING THE RCIC |
| POWER OPERATED VALVE OPERABILITY SURVEILLANCE TEST, THE VALVE MOVED TO THE |
| INTERMEDIATE POSITION AND STOPPED. STATION OPERATORS VERIFIED THAT THE |
| VALVE WAS NOT CLOSED AND ISOLATED THE RCIC SYSTEM STEAM SUPPLY AND SUCTION |
| AND DISCHARGE PATHS IN ORDER TO PREVENT SYSTEM INITIATION, EVIDENCE |
| PRESERVATION, AND EXCESSIVE CYCLING OF THE BAROMETRIC CONDENSER PUMP. |
| STATION OPERATORS ALSO VERIFIED THAT THE HIGH PRESSURE COOLANT INJECTION |
| SYSTEM WAS OPERABLE. |
| |
| TECH SPEC LCO A/S 3.5.3.A REQUIRES THE LICENSE TO RESTORE THE RCIC SYSTEM TO |
| OPERABLE STATUS WITHIN 14 DAYS OR SHUT THE PLANT DOWN. |
| |
| STATION OPERATORS ARE INVESTIGATING THE CAUSE OF THE VALVE FAILURE AND PLAN |
| TO REPAIR THE VALVE. |
| |
| THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. |
+------------------------------------------------------------------------------+