U.S. Nuclear Regulatory Commission
Operations Center
Event Reports For
01/14/1999 - 01/15/1999
** EVENT NUMBERS **
35206 35248 35259 35260 35261 35262 35263 35264 35265 35266
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 35206 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PERRY REGION: 3 |NOTIFICATION DATE: 12/30/1998|
| UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 19:03[EST]|
| RXTYPE: [1] GE-6 |EVENT DATE: 12/30/1998|
+------------------------------------------------+EVENT TIME: 16:00[EST]|
| NRC NOTIFIED BY: HENRY KELLY |LAST UPDATE DATE: 01/14/1999|
| HQ OPS OFFICER: BOB STRANSKY +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |MONTE PHILLIPS R3 |
|10 CFR SECTION: | |
|NLTR LICENSEE 24 HR REPORT | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| 24-HOUR REPORT REQUIRED BY PLANT OPERATING LICENSE DUE TO VIOLATION OF |
| TECHNICAL SPECIFICATIONS |
| |
| The licensee has discovered that a solenoid-operated isolation valve on a |
| 3/8" diameter sample line from the secondary containment was excluded from |
| the plant technical specifications (TS), and, consequently, it was not |
| subject to surveillances required by the TS. The valve is located on a |
| secondary containment atmosphere sample line which connects to the |
| post-accident sampling system. The licensee has verified that the valve is |
| closed. |
| |
| The NRC resident inspector has been informed of this event by the licensee. |
| |
| * * * UPDATE AT 2117 EST ON 01/14/99 FROM BRIAN STETSON TO S. SANDIN * * * |
| |
| The following text is a portion of a facsimile received from the licensee: |
| |
| "During the extent of condition investigation of Condition Report 98-2142, |
| it was identified that instrument vent and drain valves associated with the |
| reactor core isolation cooling system (E51) and the annulus exhaust gas |
| treatment system (M15) could fit the definition of secondary containment |
| isolation valves as discussed in Technical Specification Bases 3.6.4.2. |
| However, these valves are not surveilled and checked closed every 31 days as |
| required by Surveillance Requirement 3.6.4.2.1. There are 12 valves (3/8") |
| associated with E51, and 8 valves (1/4") associated with M15." |
| |
| The licensee plans to continue its evaluation and has informed the NRC |
| Resident Inspector. The NRC Operations Officer notified the R3DO (Gavula). |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 35248 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 01/13/1999|
| UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 10:21[EST]|
| RXTYPE: [1] GE-6 |EVENT DATE: 01/13/1999|
+------------------------------------------------+EVENT TIME: 08:35[CST]|
| NRC NOTIFIED BY: ROBERT POWER |LAST UPDATE DATE: 01/14/1999|
| HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |JIM GAVULA R3 |
|10 CFR SECTION: | |
|AESS 50.72(b)(1)(v) EMERGENCY SIREN INOP | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N N 0 Cold Shutdown |0 Cold Shutdown |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| LOSS OF HALF OF THE OFFSITE EMERGENCY SIRENS DUE TO FREEZING RAIN |
| |
| The following text is a portion of a facsimile received from the licensee: |
| |
| "10CFR50.72(b)(1)(v) requires that a facility notify the NRC Operations |
| Center during any event that results in a major loss of emergency offsite |
| response capability. Due to weather conditions causing area power outages, |
| a system test of the emergency sirens was conducted. During this test, it |
| was discovered that 22 out of 44 emergency sirens were not functioning. |
| Therefore, Clinton Power Station is making a notification pursuant to |
| 10CFR50.72(b)(1)(v)." The licensee's current site policy is to make a |
| notification of this type if less than 90% of the emergency sirens are |
| available. |
| |
| The licensee notified the NRC resident inspector. |
| |
| *** UPDATE ON 01/14/99 @ 1442 EST FROM POWERS TO GOULD *** |
| |
| As of 0930 CST, the plant restored power to all but four emergency sirens. |
| |
| The NRC resident inspector will be notified by the licensee. The R3DO |
| (Gavula) was notified by the NRC operations officer. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 35259 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: BIG ROCK POINT REGION: 3 |NOTIFICATION DATE: 01/14/1999|
| UNIT: [1] [] [] STATE: MI |NOTIFICATION TIME: 03:26[EST]|
| RXTYPE: [1] GE-1 |EVENT DATE: 01/14/1999|
+------------------------------------------------+EVENT TIME: 03:00[EST]|
| NRC NOTIFIED BY: MIKE AZURE |LAST UPDATE DATE: 01/14/1999|
| HQ OPS OFFICER: LEIGH TROCINE +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |JIM GAVULA R3 |
|10 CFR SECTION: | |
|AENS 50.72(b)(1)(v) ENS INOPERABLE | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N N 0 Decommissioned |0 Decommissioned |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| LOSS OF EMERGENCY NOTIFICATION SYSTEM (ENS) AND COMMERCIAL TELEPHONES |
| |
| At 0300, it was discovered that the FTS-2000 ENS telephone line and the |
| offsite commercial telephone lines were out of service. The cause of this |
| telephone outage is unknown at this time. However, the licensee stated that |
| there does not seem to be a trunk line problem. The licensee has contacted |
| Ameritech and a local telephone representative. Offsite communications are |
| available via the use of cellular telephones and base radios to the Michigan |
| State Police and to the licensee's power control (load dispatcher). Outside |
| calls can be made from those locations if it is necessary for the licensee |
| to relay information. |
| |
| (Call the NRC Operations Center for a licensee cellular telephone number.) |
| |
| ******************** UPDATE AT 1009 ON 01/14/99 FROM GARY RUEHLE TO TROCINE |
| ******************** |
| |
| Telephone service was restored at approximately 0930, and the ENS line |
| tested satisfactorily at 1009. The telephone outage was due to an Ameritech |
| problem. |
| |
| The NRC operations officer notified the R3DO (Gavula). |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Hospital |Event Number: 35260 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG: HAWAIIAN EYE CENTER |NOTIFICATION DATE: 01/14/1999|
|LICENSEE: HAWAIIAN EYE CENTER |NOTIFICATION TIME: 13:00[EST]|
| CITY: WAHIAWA REGION: 4 |EVENT DATE: 01/14/1999|
| COUNTY: HONOLULU STATE: HI |EVENT TIME: [HST]|
|LICENSE#: 53-18343-01 AGREEMENT: N |LAST UPDATE DATE: 01/14/1999|
| DOCKET: |+----------------------------+
| |PERSON ORGANIZATION |
| |BLAIR SPITZBERG R4 |
| |JOHN SURMEIER, EO NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: CYNTHIA SEMBRANO | |
| HQ OPS OFFICER: STEVE SANDIN | |
+------------------------------------------------+ |
|EMERGENCY CLASS: N/A | |
|10 CFR SECTION: | |
|LADM 35.33(a) MED MISADMINISTRATION | |
| | |
| | |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| LICENSEE REPORTED THAT NUMEROUS PATIENTS RECEIVED LESS THAN THE PRESCRIBED |
| Sr-90 DOSE. |
| |
| IN 1998, TWELVE (12) PATIENTS WERE DIAGNOSED AND TREATED FOR PTERYGIUM, A |
| SUPERFICIAL GROWTH ON THE LENS OF THE EYE, ELEVEN HUNDRED (1,100) RADS WAS |
| PRESCRIBED FOR EACH; HOWEVER, DUE TO THE LICENSEE NOT APPLYING A DECAY |
| FACTOR TO THE STRONTIUM-90 SOURCE, PATIENTS RECEIVED APPROXIMATELY 600 RADS. |
| THE TWO (2) EYE APPLICATORS (SERIAL #s 0302 AND 431 - EACH 100 mCi Sr-90) |
| WERE RECEIVED FROM NEW ENGLAND NUCLEAR IN MARCH 1979. THE DISCREPANCY IN |
| THE PRESCRIBED VERSUS ADMINISTERED DOSE WAS DISCOVERED DURING AN ONSITE |
| INSPECTION BY THE NRC ON 01/13/99. THE LICENSEE IS CONTINUING ITS |
| INVESTIGATION TO DETERMINE APPROPRIATE CORRECTIVE ACTIONS. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 35261 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: HARRIS REGION: 2 |NOTIFICATION DATE: 01/14/1999|
| UNIT: [1] [] [] STATE: NC |NOTIFICATION TIME: 13:06[EST]|
| RXTYPE: [1] W-3-LP |EVENT DATE: 01/14/1999|
+------------------------------------------------+EVENT TIME: 09:18[EST]|
| NRC NOTIFIED BY: MARK PALMER |LAST UPDATE DATE: 01/14/1999|
| HQ OPS OFFICER: FANGIE JONES +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |AL BELISLE R2 |
|10 CFR SECTION: | |
|ARPS 50.72(b)(2)(ii) RPS ACTUATION | |
|AESF 50.72(b)(2)(ii) ESF ACTUATION | |
|APRE 50.72(b)(2)(vi) OFFSITE NOTIFICATION | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 A/R Y 100 Power Operation |0 Hot Standby |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| AUTOMATIC REACTOR TRIP ON TRIP OF TWO OF THREE REACTOR COOLANT PUMPS AND |
| LOSS OF TWO 6.9-kV BUSES |
| |
| During relay calibration on the 'A' 6.9-kV non-safety bus, the bus was |
| unexpectedly deenergized. The 'C' 6.9-kV bus is a swing bus and was tied to |
| the 'A' 6.9-kV bus, which caused it to be deenergized also. This caused the |
| loss of two of three reactor coolant pumps, and in turn, caused an automatic |
| reactor trip from 100% power. All systems functioned as expected, all rods |
| fully inserted, and auxiliary feedwater started on low steam generator level |
| as expected. All safety systems are operable except the 'A' containment |
| hydrogen analyzer which is out of service for planned maintenance. |
| |
| The exact cause of the loss of the 6.9-kV buses is currently under |
| investigation. |
| |
| The licensee notified the NRC Resident Inspector, the State of North |
| Carolina, and the local county. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 35262 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: FITZPATRICK REGION: 1 |NOTIFICATION DATE: 01/14/1999|
| UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 13:38[EST]|
| RXTYPE: [1] GE-4 |EVENT DATE: 01/14/1999|
+------------------------------------------------+EVENT TIME: 13:11[EST]|
| NRC NOTIFIED BY: RICK PLASSE |LAST UPDATE DATE: 01/14/1999|
| HQ OPS OFFICER: STEVE SANDIN +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: UNU |CURT COWGILL RI |
|10 CFR SECTION: |JOHN STOLZ, NRR EO |
|AAEC 50.72(a)(1)(i) EMERGENCY DECLARED |FRANK CONGEL IRO |
|NOCM COMM ASST BRIEF |SULLIVAN FEMA |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| THE LICENSEE DECLARED AN UNUSUAL EVENT DUE TO A FIRE LASTING LONGER THAN 15 |
| MINUTES INSIDE THE PROTECTED AREA. (REFER TO EVENT #s 35263 AND 35264 FOR |
| RELATED EVENTS.) |
| |
| AT 1256 EST, OPERATORS RECEIVED A REPORT OF AN ONGOING FIRE IN THE VICINITY |
| OF THE HYDROGEN TANK FARM AREA APPROXIMATELY 300 FEET WEST OF THE PLANT. |
| THE SOURCE IS A HYDROGEN RELEASE. THE LOCATION OF THE SOURCE HAS NOT BEEN |
| IDENTIFIED. THE LICENSEE EVACUATED PERSONNEL IN THE AREA AND DECLARED AN |
| UNUSUAL EVENT AT 1311 EST DUE TO AN ONGOING FIRE LASTING LONGER THAN 15 |
| MINUTES. OFFSITE FIRE ASSISTANCE WAS REQUESTED FROM THE SCRIBA FIRE |
| DEPARTMENT. ALL PERSONNEL ARE ACCOUNTED FOR WITH ONE KNOWN MINOR INJURY. |
| ALL SAFETY EQUIPMENT IS AVAILABLE. BOTH 115-kV SOURCES OF OFFSITE POWER |
| WERE DEENERGIZED AS A SAFETY PRECAUTION TO ALLOW FIREFIGHTERS' ACCESS. THE |
| LICENSEE IS MAINTAINING ELECTRICAL LOADS ON GENERATOR OUTPUT WITH THE |
| STANDBY EMERGENCY DIESEL GENERATORS RUNNING UNLOADED. THE LICENSEE INFORMED |
| NEW YORK STATE AND THE NRC RESIDENT INSPECTOR. |
| |
| * * * UPDATE AT 1424 EST ON 01/14/99 * * * |
| |
| AT 1424 EST, THE NRC ENTERED THE MONITORING PHASE OF NORMAL MODE. |
| |
| * * * UPDATE AT 1500 EST ON 01/14/99 * * * |
| |
| A COMMISSIONERS' ASSISTANTS BRIEFING WAS CONDUCTED. THE FOLLOWING |
| NOTIFICATIONS WERE MADE (* OFFICE DID NOT PARTICIPATE): IRO (CONGEL AND |
| WEINSTEIN); JACKSON (MILLER); DICUS (CHAN); DIAZ (HSIA); McGAFFIGAN (BEALL); |
| MERRIFIELD (McCABE); EDO (HILTZ); DEDE (MITCHELL*); NRR EO (STOLZ); R1DO |
| (COWGILL); PAO (GILLILAND); CAO (MADDEN); SECY (BATES); SP (LARKINS); IP |
| (FAULKNER); BRIEFER (COWGILL); SRI (RASMUSSEN); AND NRR (BAWA, WONG, LONG, |
| AND CONNELL). |
| |
| * * * UPDATE AT 1730 EST ON 01/14/99 * * * |
| |
| A COMMISSIONERS' ASSISTANTS BRIEFING WAS CONDUCTED. THE FOLLOWING |
| NOTIFICATIONS WERE MADE: IRO (CONGEL), JACKSON (MILLER), DICUS (CHAN), DIAZ |
| (HSIA), McGAFFIGAN (BEALL), MERRIFIELD (McCABE), EDO (HILTZ), BRIEFER |
| (COWGILL), SRI (RASMUSSEN), AND NRR (BAWA AND WILLIAM). |
| |
| * * * UPDATE AT 2111 EST ON 01/14/99 FROM TOM KERR TO FANGIE JONES * * * |
| |
| THE LICENSEE TERMINATED THE UNUSUAL EVENT AT 2105 EST. THE LICENSEE |
| INFORMED THE NRC RESIDENT INSPECTOR. |
| |
| * * * UPDATE AT 2120 EST ON 01/14/99 * * * |
| |
| THE NRC EXITED THE MONITORING PHASE OF NORMAL MODE AT 2108 EST. THE NRC |
| OPERATIONS OFFICER NOTIFIED THE NRR EO (BOGER), IRO (CONGEL), AND FEMA |
| (CANUPP). |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 35263 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 01/14/1999|
| UNIT: [1] [] [] STATE: NY |NOTIFICATION TIME: 14:23[EST]|
| RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 01/14/1999|
+------------------------------------------------+EVENT TIME: 13:47[EST]|
| NRC NOTIFIED BY: REVETTE |LAST UPDATE DATE: 01/14/1999|
| HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: UNU |GENE KELLY R1 |
|10 CFR SECTION: |JOHN STOLZ, NRR EO |
|AAEC 50.72(a)(1)(i) EMERGENCY DECLARED |CIBOCH FEMA |
| |FRANK CONGEL IRO |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| THE LICENSEE DECLARED AN UNUSUAL EVENT DUE TO PLANT'S PROXIMITY TO A |
| HYDROGEN FIRE AT FITZPATRICK. (REFER TO EVENT #s 35262 AND 35264 FOR |
| RELATED EVENTS.) |
| |
| THE LICENSEE IS DOING A PRECAUTIONARY STAFFING OF ITS TECHNICAL SUPPORT |
| CENTER DUE TO THE FIRE AT FITZPATRICK. |
| |
| THE LICENSEE HAS NOTIFIED THE NRC RESIDENT INSPECTOR AS WELL AS STATE, |
| LOCAL, AND OTHER AGENCIES. THERE WILL BE NO PRESS RELEASE. |
| |
| * * * UPDATE AT 2139 EST ON 01/14/99 FROM STAN LUCAS TO S.SANDIN * * * |
| |
| UNIT 1 EXITED THE UNUSUAL EVENT AT 2125 EST BASED ON TERMINATION OF THE |
| FITZPATRICK UNUSUAL EVENT. |
| |
| THE LICENSEE INFORMED STATE/LOCAL AGENCIES AND THE NRC RESIDENT INSPECTOR. |
| THE NRC OPERATIONS OFFICER NOTIFIED R1DO (KELLY), NRR EO (BOGER), IRO |
| (CONGEL), AND FEMA (STEINDURF). |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 35264 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: NINE MILE POINT REGION: 1 |NOTIFICATION DATE: 01/14/1999|
| UNIT: [] [2] [] STATE: NY |NOTIFICATION TIME: 14:23[EST]|
| RXTYPE: [1] GE-2,[2] GE-5 |EVENT DATE: 01/14/1999|
+------------------------------------------------+EVENT TIME: 13:47[EST]|
| NRC NOTIFIED BY: WEAVER |LAST UPDATE DATE: 01/14/1999|
| HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: UNU |GENE KELLY R1 |
|10 CFR SECTION: |JOHN STOLZ, NRR EO |
|AAEC 50.72(a)(1)(i) EMERGENCY DECLARED |CIBOCH FEMA |
| |FRANK CONGEL IRD |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
| | |
|2 N Y 100 Power Operation |100 Power Operation |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| THE LICENSEE DECLARED AN UNUSUAL EVENT DUE TO PLANT'S PROXIMITY TO A |
| HYDROGEN FIRE AT FITZPATRICK. (REFER TO EVENT #s 35262 AND 35263 FOR |
| RELATED EVENTS.) |
| |
| THE LICENSEE IS EVACUATING PERSONNEL FROM ITS BUILDINGS LOCATED ON THE EAST |
| SIDE OF THE SITE OUTSIDE THE PROTECTED AREA FENCE. THESE BUILDINGS WERE |
| APPROXIMATELY SEVERAL HUNDRED YARDS FROM THE FIRE SITE. THIS ACTION WAS |
| RECOMMENDED BY A LOCAL OFFICIAL BASED ON THE FIRE AT THE FITZPATRICK SITE |
| WHICH BORDERS NINE MILE POINT'S EAST BOUNDARY. IT IS REPORTED THAT HYDROGEN |
| WILL BE VENTED FOR SEVERAL HOURS. WIND DIRECTION IS FROM FITZPATRICK SITE |
| TOWARDS NINE MILE POINT. |
| |
| THE NRC RESIDENT INSPECTOR WAS NOTIFIED ALONG WITH STATE, LOCAL, AND OTHER |
| GOVERNMENT AGENCIES. THE LICENSEE PLANS TO ISSUE A PRESS RELEASE. |
| |
| * * * UPDATE AT 2139 EST ON 01/14/99 FROM STAN LUCAS TO S.SANDIN * * * |
| |
| UNIT 2 EXITED THE UNUSUAL EVENT AT 2125 EST BASED ON TERMINATION OF THE |
| FITZPATRICK UNUSUAL EVENT. |
| |
| THE LICENSEE INFORMED STATE/LOCAL AGENCIES AND THE NRC RESIDENT INSPECTOR. |
| THE NRC OPERATIONS OFFICER NOTIFIED THE R1DO (KELLY), NRR EO (BOGER), IRO |
| (CONGEL) AND FEMA (STEINDURF). |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 35265 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: BROWNS FERRY REGION: 2 |NOTIFICATION DATE: 01/14/1999|
| UNIT: [] [] [3] STATE: AL |NOTIFICATION TIME: 20:26[EST]|
| RXTYPE: [1] GE-4,[2] GE-4,[3] GE-4 |EVENT DATE: 01/14/1999|
+------------------------------------------------+EVENT TIME: 16:40[CST]|
| NRC NOTIFIED BY: RODNEY NACOSTE |LAST UPDATE DATE: 01/14/1999|
| HQ OPS OFFICER: STEVE SANDIN +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |AL BELISLE R2 |
|10 CFR SECTION: | |
|AINB 50.72(b)(2)(iii)(B) POT RHR INOP | |
|NLCO TECH SPEC LCO A/S | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
| | |
| | |
|3 N Y 100 Power Operation |100 Power Operation |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| LICENSEE DECLARED HIGH PRESSURE COOLANT INJECTION (HPCI) INOPERABLE DUE TO |
| AN OIL LEAK OBSERVED DURING START OF THE PUMP. |
| |
| THE FOLLOWING TEXT IS A PORTION OF A FACSIMILE RECEIVED FROM THE LICENSEE: |
| |
| "DURING THE PERFORMANCE OF [PROCEDURE] 3-SR-3.5.1.7, HPCI MAIN AND BOOSTER |
| PUMP SET DEVELOPED HEAD AND FLOW RATE TEST, WHILE THE HPCI PUMP WAS |
| STARTING, AN OIL LEAK DEVELOPED ON [VALVE] 3-SV-73-18, HPCI STOP VALVE. ONE |
| STUD WAS FOUND SHEARED FROM THE STOP VALVE. HPCI WAS SUBSEQUENTLY DECLARED |
| INOPERABLE, AND THE APPROPRIATE [LIMITING CONDITIONS FOR OPERATION] WERE |
| ENTERED." |
| |
| THE LICENSEE IS CONDUCTING AN INVESTIGATION TO DETERMINE THE CAUSE OF THE |
| FAILURE AND THE APPROPRIATE CORRECTIVE ACTIONS. |
| |
| THE LICENSEE INFORMED THE NRC RESIDENT INSPECTOR. |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
|Power Reactor |Event Number: 35266 |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: DRESDEN REGION: 3 |NOTIFICATION DATE: 01/14/1999|
| UNIT: [] [2] [3] STATE: IL |NOTIFICATION TIME: 21:27[EST]|
| RXTYPE: [1] GE-1,[2] GE-3,[3] GE-3 |EVENT DATE: 01/14/1999|
+------------------------------------------------+EVENT TIME: 20:12[CST]|
| NRC NOTIFIED BY: SALGADO |LAST UPDATE DATE: 01/14/1999|
| HQ OPS OFFICER: FANGIE JONES +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |JAMES CREED, REG 3 IAT |
|10 CFR SECTION: |JOHN DAVIDSON, NMSS IAT |
|DDDD 73.71 UNSPECIFIED PARAGRAPH |RICHARD ROSANO, NRR IAT |
| |BRUCE BOGER, NRR EO |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
| | |
|2 N Y 100 Power Operation |100 Power Operation |
|3 N Y 100 Power Operation |100 Power Operation |
+------------------------------------------------------------------------------+
EVENT TEXT
+------------------------------------------------------------------------------+
| There was an unauthorized entry into the protected area, and immediate |
| compensatory measures were taken upon discovery. (Contact the NRC |
| Operations Center for additional details.) |
| |
| The licensee notified the NRC Resident Inspector. |
+------------------------------------------------------------------------------+