U.S. Nuclear Regulatory Commission
Operations Center
Event Reports For
08/08/2000 - 08/09/2000
** EVENT NUMBERS **
37212 37213 37214
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|Power Reactor |Event Number: 37212 |
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| FACILITY: PEACH BOTTOM REGION: 1 |NOTIFICATION DATE: 08/08/2000|
| UNIT: [] [3] [] STATE: PA |NOTIFICATION TIME: 01:24[EDT]|
| RXTYPE: [2] GE-4,[3] GE-4 |EVENT DATE: 08/07/2000|
+------------------------------------------------+EVENT TIME: 21:26[EDT]|
| NRC NOTIFIED BY: WINGFIELD |LAST UPDATE DATE: 08/08/2000|
| HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |LAWRENCE DOERFLEIN R1 |
|10 CFR SECTION: | |
|ARPS 50.72(b)(2)(ii) RPS ACTUATION | |
|AESF 50.72(b)(2)(ii) ESF ACTUATION | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
| | |
|3 A/R Y 100 Power Operation |0 Hot Shutdown |
| | |
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EVENT TEXT
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| REACTOR SCRAM FROM 100% POWER ON A FALSE LOW REACTOR WATER LEVEL INDICATION |
| |
| The Unit experienced an automatic reactor scram when an instrument line |
| "root" valve failed causing a water leak which resulted in a false low |
| reactor water level signal indication to be sensed by the RPS. The water |
| leak was immediately isolated by the ESF actuation of the Excess Flow Check |
| Valve in the same reactor instrumentation line. All rods fully inserted, no |
| ECCS injection occurred, no relief valves lifted and all safety systems |
| responded correctly. The plant also had actuation of the Primary |
| Containment Isolation System following the reactor scram. |
| |
| The NRC Resident Inspector will be notified. |
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|Power Reactor |Event Number: 37213 |
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| FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 08/08/2000|
| UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 10:42[EDT]|
| RXTYPE: [1] GE-6 |EVENT DATE: 08/08/2000|
+------------------------------------------------+EVENT TIME: 08:39[CDT]|
| NRC NOTIFIED BY: SCHOTTEL |LAST UPDATE DATE: 08/08/2000|
| HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |RONALD GARDNER R3 |
|10 CFR SECTION: | |
|AENS 50.72(b)(1)(v) ENS INOPERABLE | |
|AARC 50.72(b)(1)(v) OTHER ASMT/COMM INOP | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N N 0 Cold Shutdown |0 Cold Shutdown |
| | |
| | |
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EVENT TEXT
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| PLANT HAS LOST ENS, STATE NOTIFICATION PHONE LINES AND LOCAL COMMERCIAL |
| PHONE LINES. |
| |
| THE ENS LINES, DIRECT LINES TO THE STATE, AND LOCAL COMMERCIAL LINES HAVE |
| BEEN CUT RESULTING IN THE LOSS OF THE USE OF THESE PHONE SYSTEMS. HOWEVER, |
| THEY DO HAVE OPERABLE FOREIGN EXCHANGE B/U PHONES AVAILABLE, SO THAT |
| EMERGENCY RESPONSE CAPABILITY IS NOT AFFECTED. THE TELEPHONE COMPANY IS |
| AWARE OF THE PROBLEM AND IS CURRENTLY WORKING ON IT. THE LICENSEE ALSO HAS |
| A SATELLITE PHONE AVAILABLE |
| |
| THE NRC RESIDENT INSPECTOR AND THE STATE HAVE BEEN INFORMED. |
| |
| * * * UPDATE 1453 8/8/2000 FROM SCHOTTEL TAKEN BY STRANSKY * * * |
| |
| All telephone lines have been restored. The NRC resident inspector has been |
| informed. Notified R3DO (Gardner). |
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|Power Reactor |Event Number: 37214 |
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| FACILITY: PERRY REGION: 3 |NOTIFICATION DATE: 08/08/2000|
| UNIT: [1] [] [] STATE: OH |NOTIFICATION TIME: 21:35[EDT]|
| RXTYPE: [1] GE-6 |EVENT DATE: 08/08/2000|
+------------------------------------------------+EVENT TIME: 18:44[EDT]|
| NRC NOTIFIED BY: FREDERICK SMITH |LAST UPDATE DATE: 08/08/2000|
| HQ OPS OFFICER: BOB STRANSKY +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |RONALD GARDNER R3 |
|10 CFR SECTION: | |
|AESF 50.72(b)(2)(ii) ESF ACTUATION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 99 Power Operation |99 Power Operation |
| | |
| | |
+------------------------------------------------------------------------------+
EVENT TEXT
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| AUTOSTART OF ANNULUS EXHAUST GAS TREATMENT SYSTEM FAN DURING TESTING |
| |
| "During performance of surveillance testing, the lifting of an incorrect |
| lead caused a low flow condition on the in service AEGTS fan. This caused |
| the auto start of the standby AEGTS fan. No low flow alarm was received on |
| the in service fan, but the system functioned properly." |
| |
| The NRC resident inspector has been informed of this event by the licensee. |
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