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Nine Mile Point 2
3Q/2008 Plant Inspection Findings


Initiating Events

Significance:a graphic of the significance Sep 29, 2008
Identified By: NRC
Item Type: FIN Finding
Inadequate Maintenance Practices Result in a Plant Transient
A self-revealing finding was identified on July 14, 2008, when inadequate maintenance practices, during replacement and troubleshooting of a Unit 2 radioactive waste sump pump, caused an electrical transient that resulted in the loss of numerous plant components and required a power reduction. The inadequate maintenance practices included failure to perform post-maintenance testing and continuation of troubleshooting despite having obtained results that were not consistent with the troubleshooting plan. This issue was entered into NMPNS’s corrective action program for evaluation.

The finding was greater than minor because it affected the human performance attribute of the Initiating Events cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. The finding was evaluated in accordance with IMC 0609 and determined to be of very low safety significance because the finding did not contribute to both the likelihood of a rector trip and the likelihood that mitigation equipment or functions would not be available, and did not screen as potentially risk significant due to external events. The finding had a cross-cutting aspect in the area of human performance because NMPNS did not appropriately plan the pump troubleshooting activity by incorporating abort criteria.
Inspection Report# : 2008004 (pdf)

Significance:a graphic of the significance Jul 31, 2008
Identified By: NRC
Item Type: FIN Finding
Failure to perform a technical evaluation or restore a nonconformance to the original design requirement
A self revealing Green finding was identified because Constellation failed to either perform a technical evaluation or restore a nonconforming condition to the original design requirement which resulted in a failure of the Unit 2 instrument air piping on March 26, 2008. The nonconforming condition was unannealed red brass piping which was installed in the Unit 2 instrument air system. Subsequent to the piping failure, the licensee performed corrective actions which included replacing all unannealed red brass piping that is not protected by an excess flow check valve and began closely monitoring for water in the instrument air system. Additionally, the licensee plans to replace the instrument air dryers and replace the remaining unannealed red brass piping in the instrument air system.

The finding was greater than minor because it is associated with the design control attribute of the initiating events cornerstone and the associated cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations in that a loss of instrument air could cause a plant scram with complications. The finding was determined to be of very low safety significance in accordance with IMC 0609, Appendix A, "Determining the Significance of Reactor Inspection Findings for At-Power Situations," based on a Phase 3 analysis. The Region I senior reactor analyst (SRA) used the Nine Mile Point Unit 2 Standardized Plant Analysis Risk (SPAR) model to determine the risk significance.
Inspection Report# : 2008007 (pdf)

Significance:a graphic of the significance Jun 30, 2008
Identified By: NRC
Item Type: FIN Finding
Untimely Corrective Action for IA System Corrosion Resulted in Reactor Feedwater Valve Malfunction
A self-revealing finding was identified on April 18, 2008, when NMPNS failed to take appropriate corrective actions to address corrosion products in the instrument air (IA) system in a timely manner, which led to an accumulation of water in the Unit 2 IA system. As a result, water intrusion into the air operator for the 'B' reactor feedwater pump recirculation valve caused the valve to open during plant power ascension, causing a reduction in feedwater flow to the reactor and thereby challenging plant stability. As immediate corrective action, operators secured power ascension and isolated the recirculation valve.

The finding was greater than minor because it was associated with the equipment performance attribute of the Initiating Events cornerstone and adversely affected the cornerstone objective to limit the likelihood of those events that upset plant stability and challenge critical safety functions during shutdown as well as power operations. The finding was evaluated in accordance with IMC 0609, Attachment 4, and determined to be of very low safety significance per the SDP Phase one determination because the finding did not contribute to both the likelihood of a reactor trip and the likelihood that mitigation equipment or functions would not be available, and it did not screen as potentially risk significant due to external events. The finding had a cross cutting aspect in the area of problem identification and resolution because NMPNS did not take appropriate corrective actions to address corrosion products in the IA system in a timely manner (P.1.d per IMC 0305).

Inspection Report# : 2008003 (pdf)


Mitigating Systems

Significance:a graphic of the significance Sep 29, 2008
Identified By: NRC
Item Type: NCV NonCited Violation
Incorrect Risk Assessment for RCIC Unavailability
An NRC-identified non-cited violation (NCV) of 10 CFR 50.65(a)(4) was identified for inaccurate risk assessments completed for August 5 and 6, 2008. Specifically, the unavailable reactor core isolation cooling (RCIC) system was not properly incorporated into the risk assessment. The cause was determined to be that an error had been made while entering a change to the risk monitor computer software, which resulted in RCIC incorrectly being assigned a zero risk importance. As corrective actions, the modeling of RCIC was corrected and a verification of all mapping codes used in the risk monitor was performed.

The finding was greater than minor because the risk assessment for RCIC system maintenance was inadequate due to inaccurate information that was provided to the risk assessment tool. As a result, the overall elevated plant risk, when correctly assessed, put the plant into a higher licensee-established risk category. The finding was evaluated in accordance with IMC 0609, Appendix K, and determined to be of very low safety significance because the incremental core damage probability deficit (ICDPD) was less than 1E-6. The finding had a cross-cutting aspect in the area of human performance because NMPNS did not appropriately plan work activities by incorporating valid risk insights.

Inspection Report# : 2008004 (pdf)

Significance:a graphic of the significance Jun 30, 2008
Identified By: NRC
Item Type: NCV NonCited Violation
Failure to Appropriately Evaluate the Effect of Accelerated Aging of J-10 Relays
A self-revealing non-cited violation (NCV) of 10 CRF 50, Appendix B, Criterion XVI, "Corrective Action," was identified on March 22, 2008, when the Unit 2 Division I emergency diesel generator (EDG) service water (SW) return isolation valve failed to fully open following a start of the Division I EDG, thus challenging the EDG's ability to perform its safety function. The motor operated valve (MOV) malfunction was due to age-related failure of the J-10 relay in the MOV control circuit. The susceptibility of J-10 relays to age-related failure had been previously identified; however, NMPNS did not take action to establish a maintenance strategy to replace these relays prior to failure. As corrective action, the EDG was declared inoperable, the J-10 relay was replaced, and an extent of condition review was initiated.

The finding was greater than minor because it was associated with the equipment performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The finding was evaluated in accordance with IMC 0609, Attachment 4, and determined to be of very low safety significance per the SDP Phase one determination because the finding was not a design or qualification deficiency, did not represent a loss of a system/train safety function, and did not screen as potentially risk significant due to external events.

Inspection Report# : 2008003 (pdf)

Significance:a graphic of the significance Jun 30, 2008
Identified By: NRC
Item Type: NCV NonCited Violation
Failure to Properly Control Operations Staff Overtime
An NRC-identified non-cited violation (NCV) of Unit 1 Technical Specification (TS) 6.2.2 and Unit 2 TS 5.2.2, "Unit Staff," was identified for not properly implementing and maintaining procedures for controlling plant staff work hours of personnel performing safety-related activities. Specifically, over 400 overtime deviations were approved between July 2007 and April 2008 for Operations personnel to work greater than procedurally established work hour limits for routine outage support activities during outages and other reasons not permitted by TS. Corrective actions were being developed to increase qualified operator levels.

The finding was greater than minor because, if left uncorrected, it would become a more significant safety concern. Specifically, the excessive work hours would increase the likelihood of human errors during plant activities and response to plant events. The finding has been reviewed by NRC management in accordance with IMC 0609, Appendix M, "Significance Determination Process Using Qualitative Criteria." Although the increased likelihood of human error would adversely affect the station’s defense-in-depth, the violation was determined to be of very low significance because no significant events or human performance issues were directly linked to personnel fatigue as a result of the hours worked. The issue had a cross-cutting aspect in the area of human performance because the licensee did not use conservative assumptions in decision making, in that, the consequences of the high number of overtime deviations were not fully considered and the possible unintended consequences evaluated. (H.1.b per IMC 0305).

Inspection Report# : 2008003 (pdf)

Significance:a graphic of the significance Jun 30, 2008
Identified By: NRC
Item Type: NCV NonCited Violation
Repetitive Improper Authorization and Evaluation of Overtime Deviations
A non-cited violation (NCV) of Unit 1 Technical Specification (TS) 6.2.2 and Unit 2 TS 5.2.2, "Unit Staff," was identified by the inspectors for a recurring trend of operations personnel being required to stand 24 hour shifts in order to ensure adequate shift coverage. There were eight occurrences between May 2007 and May 2008. Several of these overtime deviations were not properly authorized or documented in accordance with station procedures as required by TS. Corrective actions were being developed to increase qualified operator levels.

The finding was greater than minor because, if left uncorrected, it would become a more significant safety concern. Specifically, the excessive work hours would increase the likelihood of human errors during plant activities and response to plant events. The finding has been reviewed by NRC management in accordance with IMC 0609, Appendix M, "Significance Determination Process Using Qualitative Criteria." Although the increased likelihood of human error would adversely affect the station’s defense-in-depth, the violation was determined to be of very low significance because no significant events or human performance issues were directly linked to personnel fatigue as a result of the hours worked. The issue has a cross-cutting aspect in the area of problem identification and resolution because NMPNS failed to periodically trend and assess information from the corrective action program and other assessments in the aggregate to identify programmatic and common cause problems
Inspection Report# : 2008003 (pdf)

Significance:a graphic of the significance Mar 31, 2008
Identified By: NRC
Item Type: NCV NonCited Violation
Failure to Correctly Perform Procedure Caused Inadvertent Isolation of RCIC Steam Supply
A self-revealing, non-cited violation (NCV) of Technical Specification (TS) 5.4, "Procedures," was identified on January 14, 2008, when technicians improperly performed a surveillance procedure which resulted in isolation of the Unit 2 RCIC system. Specifically, while performing a test of the area temperature instruments that provide high temperature isolation signals for the main steam system, technicians erroneously disconnected an electrical lead associated with the RCIC leak detection system. This resulted in an automatic isolation of the RCIC system steam supply and the unavailability of RCIC for approximately four hours. Operators immediately recognized the error and halted the surveillance procedure. Technicians reconnected the lead and operators restored RCIC to a normal standby lineup.

The finding was greater than minor because it was associated with the human performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The finding was determined to be of very low safety significance in accordance with IMC 0609, Appendix A, "Determining the Significance of Reactor Inspection Findings for At-Power Situations," based on a Phase 3 analysis. The Region I senior reactor analyst (SRA) used the Nine Mile Point Unit 2 Standardized Plant Analysis Risk (SPAR) model and the actual out-of-service time to determine the risk significance. This finding had a cross-cutting aspect in the area of human performance because of the ineffective use of human error prevention techniques (H.4.a per IMC 0305). (Section 1R22)

Inspection Report# : 2008002 (pdf)

Significance:a graphic of the significance Dec 29, 2007
Identified By: NRC
Item Type: NCV NonCited Violation
Inadequate RCIC Room Temperature Channel Checks
An NRC-identified NCV of Unit 2 TS 3.3.6.1, "Primary Containment Isolation Instrumentation," occurred when NMPNS failed to perform Technical Specification (TS) required channel checks of the reactor core isolation cooling (RCIC) room area temperature instruments. This resulted in a failure to detect that the Division 1 instrument was malfunctioning. Immediate corrective actions were to replace the defective temperature instrument and to perform instrument cross-checks as a part of channel checks.

The finding was greater than minor because it resulted in an instrument malfunction not being promptly identified. The finding affected the equipment performance attribute of the Mitigating Systems cornerstone to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The impact of the 2ICS*TE16A malfunction was that it reduced the amount of time that would be available for operators to bypass the RCIC room area high temperature isolation to maintain RCIC operability during a station blackout event. The finding was evaluated in accordance with IMC 0609, Appendix A, and determined to be of very low safety significance (Green) per the SDP Phase one determination because the finding was not a design or qualification deficiency, did not represent a loss of system safety function or safety function of a single train, and did not screen as potentially risk significant due to external events. This finding had a cross-cutting aspect in the area of problem identification and resolution because NMPNS did not identify the inadequate channel checks in a timely manner (P.1.a per IMC 0305). (Section 1R15)

Inspection Report# : 2007005 (pdf)

Significance:a graphic of the significance Dec 29, 2007
Identified By: NRC
Item Type: NCV NonCited Violation
Loss of Shutdown Cooling due to Inadequate Maintenance Planning
A self-revealing NCV of Unit 2 TS 5.4, "Procedures," occurred when NMPNS failed to adequately implement procedure GAP-PSH-01, “Work Control,” while Unit 2 was in the refueling mode. Specifically, an unanticipated loss of shut down cooling (SDC) occurred because operators had not adequately assessed the operational impact of emergent maintenance to test a degraded reactor protection system (RPS) cable. As a result, establishing the electrical isolation for this maintenance initiated a Division 2 primary containment isolation system (PCIS) Group 5 isolation, which caused the associated isolation valve in the common SDC suction line to close. Operators promptly recognized the cause and restored shutdown cooling to service.

The finding was greater than minor because it was associated with the equipment performance attribute of the Mitigating Systems cornerstone and adversely affected the cornerstone's objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. The finding was evaluated in accordance with IMC 0609, Appendix G, “Shutdown Operations Significance Determination Process." The finding was determined to be of very low safety significance (Green) because, although the finding resulted in there being less than one loop of RHR in SDC operation, it did not increase the likelihood of a loss of RCS inventory, degrade the ability to terminate a leak path or add RCS inventory if needed, or degrade the ability to recover decay heat removal. This finding had a cross-cutting aspect in the area of human performance because NMPNS failed to adequately assess the impact of the emergent work activity on plant operations (H.3.b per IMC 0305). (Section 1R20)

Inspection Report# : 2007005 (pdf)


Barrier Integrity


Emergency Preparedness


Occupational Radiation Safety


Public Radiation Safety


Physical Protection

Although the NRC is actively overseeing the Security cornerstone, the Commission has decided that certain findings pertaining to security cornerstone will not be publicly available to ensure that potentially useful information is not provided to a possible adversary. Therefore, the cover letters to security inspection reports may be viewed.


Miscellaneous

Last modified : November 26, 2008