A.1 | Name of your facility: |
| 3M Brownwood
|
A.2 | Name of your parent company: |
| 3M Company
|
A.3 | Facility contact person for the Performance Track program: |
|   Name: | Mr. James Kotsmith |
|   Title: | Senior Environmental Engineer |
|   Phone: | (651) 778-4263 |
|   Fax: | (651) 778-7203 |
|   Email: | jrkotsmith@mmm.com |
A.4 | Facility location: |
|   Street Address: | US Highway 377 |
|   Address Cont: | |
|   City: | Brownwood |
|   State: | TX |
|   Zip Code: | 76801 |
| Mailing address (if different from above): |
|   Mailing Address: | P.O. Box 33331 |
|   Address Cont: | Bldg. 42-2E-27 |
|   City: | St. Paul |
|   State: | MN |
|   Zip Code: | 55133-3331 |
A.5 | Facility's website address (if any): |
| http://mmm.com |
A.6 | Number of employees (full-time equivalents) who currently work in the facility: |
| 500-1,000 |
A.7 | North American Industrial Classification System (NAICS) Code(s) that is(are) used to classify business at the facility: |
| 326113  327212       |
A.8 | In your application and, perhaps, in previous annual performance reports, you described what your facility does or makes. Have there been any (additional) changes to your facility's list of products and/or activities? If yes, please list them here: |
| No Changes |
|
|
A.9 | Have the environmental requirements applicable to your facility changed during this reporting period? If yes, please describe these changes here. |
| No Changes |
| |
B.1.d | (Optional) If you would like to describe any other audits or inspections that were conducted at your facility, please do so here.
| |
|
The following agency inspections were conducted in 2002:
-City of Brownwood Wastewater Inspection - March 2002
-TCEQ RCRA Waste Inspection - May 2002
-TCEQ Air Inspection - May 2002
| |
B.1.e | Briefly summarize corrective actions taken and other improvements made as a result of your EMS assessments and compliance audits.
| |
|
-Provided additional training to affected employees
-Updated procedures to improve operational control
-Improved document control access to all employees
-Completed change for new raw material use
-Updated quality testing procedure
-Revised contact lists with updated personnel
-Revised plant figures and maps as necessary
| |
B.1.f | Has your facility corrected all instances of potential non-compliance and EMS non-conformance identified during your audits and other assessments? | |
| Yes
| |
| If no, please explain your plans to correct these instances. | |
|
| |
B.1.g | When was the last Senior Management review of your EMS completed? | |
| September  2002 | |
| Who was the senior manager present at the review? | |
| Name: Mr. Fred B. Kelly | |
| Title: Environmental Specialist
| |
B.2.a | ISO 14001 Certification. Is your facility currently certified to ISO 14001?
| |
| Yes
| |
B.2.b | Is your facility a Responsible Care-certified facility? |
|
|
B.3 | Environmental Aspects Identification. When did your facility last conduct a systematic identification and/or review of your environmental aspects?
| |
| September  2002
| |
B.4 | Progress Toward Achieving Objectives and Targets. In the table below, please provide a narrative summary of progress made toward EMS objectives and targets other than those reported as Environmental Performance Commitments in Section C. You may limit the summary to environmental aspects that are significant and towards which progress has been made during the reporting year. Do you have additional environmental aspects to report? Yes
| |
|
Environmental Aspect | Progress Made This Year (e.g., quantitative or qualitative improvements, activities conducted) |
Total Energy Use | Energy consumption was reduced by 69,000 MMBTU/yr through the optimization of thermal oxidizers and process heating equipment at the facility. |
Total Solid Waste | The facility implemented several yield improvement projects, including raw material substitution, to reduce solid waste by 316 tons. |
Total Solid Waste | The facility installated a dry material loading system to reduce solid waste by 50 tpy. |
Emissions of VOCs/Total Solid Waste | Several process improvement and reformulation projects resulted in the reduction of 10 tpy of VOCs and 580 tons of solid waste. |
|