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DEPARTMENT OF LABOR MINE SAFETY AND HEALTH ADMINISTRATION Metal and Nonmetal Mine Safety and Health REPORT OF INVESTIGATION Underground Metal Mine (Zinc) Fatal Fall of Back Accident May 31, 2008 Balmat Mine No. 4 & Mill St. Lawrence Zinc Company, LLC Gouverneur, St. Lawrence County, New York Mine I.D. No. 30-01185 Investigators Rodney L. Rice Mine Safety and Health Inspector Lynn D. Allen Mine Safety and Health Inspector Paul L. Tyrna Mining Engineer Originating Office Mine Safety and Health Administration Northeast District Thorn Hill Industrial Park 547 Keystone Drive, Suite 400 Warrendale, Pennsylvania 15086-7573 James R. Petrie, District Manager OVERVIEW
Willard P. Clewis, Jr., miner-1, age 40, was fatally injured on May 31, 2008, when a large rock fell and struck him. Clewis and a coworker were drilling a round at the face in a vent drift. Clewis was attempting to retrieve a drill bit from a hole at the face when the rock fell from the back. The other miner was on the outby side of the drift and was not injured. The accident occurred because adverse ground conditions encountered during the mining cycle were not addressed by management. Management provided a ground control plan listing necessary ground support materials to control adverse ground but did not ensure that the plan was implemented in the vent drift. GENERAL INFORMATION
Balmat No. 4 Mine & Mill, an underground lead-zinc mine owned and operated by St. Lawrence Zinc Company, LLC, was located approximately eight miles south/southwest of Gouverneur, St. Lawrence County, New York. The principal operating official was Michael J. Lawler, president and COO. The mine operated various shifts of eight to ten hours, 24 hours per day, seven days per week. Total employment was 222 persons. Ore was drilled and blasted from multiple drifts. Material was loaded from the faces using load-haul-dumps (LHDs) and front-end loaders. Haul trucks and LHDs transported the material to a dump station. It was sent through a jaw crusher and stored in skip bins. The material was hoisted to dump bins on the surface and processed in the mill and sold to industry for subsequent use. The last regular inspection was completed on April 18, 2008. DESCRIPTION OF THE ACCIDENT
During the three days prior to the accident, Willard P. Clewis, Jr. (victim), miner-1, and Richard R. Aldridge, Jr., general utility-1, started a project to widen a 4-foot by 7-foot vent drift on the 2100 level. They drilled, blasted, and mucked the first round but did not install roof bolts or screen mesh before they drilled three holes for the second round. On the day of the accident, Clewis and Aldridge reported to work at 6:00 a.m., their normal starting time. They went to the vent drift and Aldridge checked the air and water lines for leaks. Clewis began drilling at the top of the face to finish the row he had started the previous day. About 10:00 a.m., Clewis told Aldridge that the bit came off the end of the drill steel. He asked Aldridge to get a tamping pole to retrieve the bit. Upon receiving the tamping pole, Clewis used a knife to sharpen the end. Aldridge went to the entrance of the drift and began straightening up hoses and water lines when he heard a loud noise. When Aldridge looked toward the face, he saw a large section of rock had fallen from the back pinning Clewis. Aldridge called Clewis several times but he did not respond. Aldridge called Scott Zeller, hoist operator, on the mine phone for help. Shortly afterward, miners and mine rescue team members arrived and checked Clewis but he was non-responsive. They used air bags, scaling bars, and timbers to free the victim from the rock. Clewis was transported to the surface and then to a local hospital where he was pronounced dead by the attending physician. The cause of death was attributed to crushing injuries. INVESTIGATION OF THE ACCIDENT
The Mine Safety and Health Administration (MSHA) was notified of the accident at 11:37 a.m. on May 31, 2008, by a telephone call from Douglas L. Beachard, director of human resources, to James R. Petrie, district manager. MSHA was not notified immediately notified and a non-contributory citation was issued. An order was issued under the provisions of Section 103(k) of the Mine Act to ensure the safety of miners. An investigation was started the same day. MSHA's accident investigation team traveled to the mine, made a physical inspection of the accident scene, interviewed employees, and reviewed documents and work procedures relevant to the accident. MSHA conducted the investigation with the assistance of mine management, employees, miners' representative, and the New York State Police. DISCUSSION
Geology The mine was located within the Balmat-Edwards Zinc mining district. At the time of the accident, the mine had 50 active faces operating at depths up to 3,300 feet within an approximate area of two square miles. Development of the mine began in 1972 with ore extracted from multiple ore bodies. Regionally, the area encompassing the mine was known as the Adirondack lowlands, an area underlain by a series of complexly folded Precambrian metamorphic (amphibolite faces) rocks near the western edge of the Adirondack Massif. The rocks were part of the Grenville supergroup and consisted primarily of marble and gneiss. The ore bodies of the mine were associated with the Sylvia Lake syncline, a doubly plunging recumbent fold with a highly complex structure resulting from at least four phases of deformation. Fourteen rock units were differentiated within the syncline, five of which were associated with the ore bodies. The Sylvia Lake and lower Fowler ore bodies were contained in unit 11 which was composed of calcitic and dolomitic marble, quartz, and diopside. The upper Fowler was contained in units 7, 8, 9 and a small portion of unit 10. The Mud Pond was contained in units 6, 7, and 8 with unit 6 being composed of a complicated silicated marble that had been subdivided into about 12 subunits. In general, the ore bodies were lenticular in shape with cross-sectional dimensions of tens of feet by hundreds of feet and lengths of up to 6,000 feet along the direction of the plunge of the folds. The ore tended to be located within faulted tectonic extension joints formed within the axial plane of the folds. The ore itself consisted of nearly pure sphalerite with varying amounts of pyrite and minor galena. A series of inclined spiral ramps were developed to access the successively deeper horizontal drift levels. Designed dimensions of the drifts and haulage ways generally ranged from 10 feet by 12 feet to 14 feet by 15 feet. Actual dimensions were sometimes greater in order to accommodate large equipment or in production drifts to maximize the extraction of the non-uniformly shaped ore body. Location of the Accident The accident occurred in a vent drift on the 2100 level approximately 614 feet from the No. 4 Shaft and approximately 1,380 feet below the surface (Figure 1). The vent drift comprised one leg of a triangular development configuration and connected an old raised bore station and the access drift to the old No. 2 Mine. The access drift served as the secondary escapeway for the No. 4 Mine. The ground fell in a single slab that broke into three large pieces and several smaller pieces upon impact. The individual slabs measured 8.5 feet by 4.0 feet by 14 inches thick; 7.0 feet by 1.6 feet by 9 inches thick; and 9.0 feet by 4.0 feet by 10 inches thick. The combined weight of the material was estimated to be roughly 3.3 tons. The ground, ribs, and floor at this drift were composed of bright white, coarsely crystalline dolomitic marble referred to as "Bed 12." According to mine geologists, this rock unit was highly susceptible to spalling. Ground Support Primary ground support used in development drifts consisted of 5-foot, 39-mm split sets installed in conjunction with 6-inch by 6-inch bearing plates, through 5-foot by 9-foot mats of 6-gauge galvanized welded wire mesh oriented transversely to the drift. For each mat, the installed bolt pattern was three split sets along the front and side edges with two split sets in the middle. Each successive mat was overlapped with the trailing edge pinned by driving 2-foot long split sets into the last row of 5-foot long split sets. Supplemental supports used were 7/8-inch diameter, grade 75 fully grouted Dywidag threadbar cut to length (typically 12-foot) from 24-foot stock. Primary support in production drifts was the same as that used in development drifts with the exception of small drifts (8 feet high) where 5-foot long Swellex® bolts were used. Supplemental support in production areas included 8-foot long Swellex® bolts and up to 20 feet long, 0.6-inch diameter cement grouted cable bolts (typically double cased). The evaluation of the 2100 level vent drift revealed that no action had been taken to support the loose, drummy sounding, material in the back of the drift. There were separations or cracks present over the entrance into the drift but no support was installed. Ground Support Policy On May 21, 2007, mine management issued Policy BMP-067 "Ground Support Using Hand Held Pneumatic Drills." The policy outlined the ground support procedures and materials to be used and installed in areas with conditions similar to the vent drift on the 2100 level. In accordance with the policy, miners were instructed to safely scale down material before the ground was bolted or screened. Miners were to start from the last row of permanent supports and fasten wire mesh in place by inserting 2-foot split sets into the existing 5-foot split sets. Holes were to be drilled one at a time perpendicular to the ground to be supported. Wire mesh was to be applied from the sidewall arch or shoulder completely across the drift to the opposing sidewall arch or shoulder. The policy required voids between the mesh and the back to be minimized and bolts spaced accordingly. The sidewalls were to be bolted if necessary. This ground support policy was not followed in the vent drift on the 2100 level where the accident occurred. Miners worked in this area for four days but management did not ensure that adequate ground support was installed. Equipment At the time of the accident, the victim was using a Midwestern Machine Model PHQ250 Jackleg drill with a 51" retractable air leg. He was standing atop a 2 ½ feet high pre-fabricated drill platform to access the upper row of holes in the face. Training and Experience Willard P. Clewis, Jr., victim, had two years, two months, two days mining experience. Richard P. Aldridge had three weeks mining experience and had worked underground for four days. Clewis and Aldridge had received training in accordance with 30 CFR, Part 48. ROOT CAUSE ANALYSIS
A root cause analysis was performed and the following root causes were identified: Root Cause: Ground support was not installed in the vent drift on the 2100 level. Corrective Action: Ground support should be used where conditions or mining experience in similar ground conditions in the mine indicate that it is necessary. Root Cause: Management policies, procedures, and controls were not being followed. Specifically, the ground was not supported in the vent drift on the 2100 level as specified by the company's ground support policy to protect persons where they worked or traveled. Corrective Action: Management should ensure that established policies, procedures, and controls are followed. Miners should be trained to install ground support in adverse conditions as required. CONCLUSION
The accident occurred because management failed to ensure that adverse ground conditions encountered during the mining cycle were addressed. Management provided a ground control plan listing ground support materials to control adverse ground but did not ensure that the plan was implemented in the vent drift. ENFORCEMENT ACTIONS
Order No. 6054408 was issued on June 1, 2008, under the provisions of Section 103(k) of the Mine Act:
Citation No. 6054415 was issued on July 7, 2008 under the provisions of Section 104(d)(1) of the Mine Act for a violation of 30 CFR 57.3360:
Related Fatal Alert Bulletin: APPENDIX A
Persons Participating in the Investigation Hudson Bay Mining and Smelting Co., Limited (parent company)
Ian Cooper .......... safety & health director
Danny Weldon .......... senior safety engineer Gary Walton .......... electrical superintendent Marty Spilman .......... safety trainer Mike Ellis .......... mine trainer Ted Parsons .......... senior internal auditor Robert Baderman .......... miners' representative
Lynn D. Allen .......... mine safety and health inspector Paul L. Tyrna .......... mining engineer |
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