skip navigation links 
 
 Search Options 
Index | Site Map | FAQ | Facility Info | Reading Rm | New | Help | Glossary | Contact Us blue spacer  
secondary page banner Return to NRC Home Page

Morning Report for November 2, 1999

                       Headquarters Daily Report

                         NOVEMBER 02, 1999

***************************************************************************
                    REPORT             NEGATIVE            NO INPUT
                    ATTACHED           INPUT RECEIVED      RECEIVED

HEADQUARTERS        X                                      
REGION I                               X                   
REGION II                              X                   
REGION III                             X                   
REGION IV                              X                   
PRIORITY ATTENTION REQUIRED  MORNING REPORT - HEADQUARTERS NOV. 02, 1999

MR Number: H-99-0096

                           NRR DAILY REPORT ITEM
                            SIGNIFICANT EVENTS



Subject: Scram and Partial Loss of Vital Power at Indian Point, Unit 2,
         Classified As A Significant Event

The Indian Point, Unit 2, August 31, 1999 event is classified as a       
Significant Event for the NRC Performance Indicator Program. The bases   
for this classification were the number of complications that resulted   
and produced unnecessary burdens on licensees operational personnel      
coupled with the lapses in configuration control and management oversight
that the event demonstrated.                                             
                                                                         
On August 31, 1999, at 2:31 p.m., the Indian Point Unit 2 reactor tripped
from 99 percent power, the trip indication was Over-Temperature          
Delta-Temperature. About three minutes after the reactor trip, the normal
offsite power breakers to all four 480 volt vital buses tripped; all     
three emergency diesel generators (EDGs) started and began to load. A    
short time later, the 23 EDG output breaker tripped, leaving the 6A vital
bus de-energized. This resulted in a loss of power to one of the two     
motor-driven auxiliary feedwater pumps, to battery charger 24 and to some
emergency core cooling components. The bus remained de-energized while   
technicians prepared tagouts and checked for a suspected bus fault which 
could have caused the loss of power. Battery 24 discharged over the next 
seven hours causing a loss of power to the loads on dc panel 24 and on ac
instrument bus 24. The loss of the dc bus rendered half of the bleed and 
feed capability of the unit inoperable if it had been required and       
complicated the emergency feedwater flow control process. The loss of the
ac instrument bus disabled most control room annunciators for safety     
related systems. The next day, about 1:00 p.m., vital bus 6A was         
re-energized using the EDG; by 9:00 p.m., normal offsite power had been  
restored to all buses and the three EDGs secured.                        
                                                                         
On September 1, 1999, the NRC initiated an Augmented Team Inspection to  
examine the circumstances surrounding the event principally because the  
event was complicated by significant, unexpected system interactions     
involving safety related equipment; also, the team was to examine the    
adequacy of the licensee's response to the event particularly the vital  
bus power restoration efforts--the delays in which led to significant    
additional complication of the operators' efforts to stabilize the plant.
The team report is provided in Inspection Report 50-247/99-08 dated      
October 19, 1999.                                                        
                                                                         
The team found that a primary cause of the event was inadequacy in       
configuration control management; the loss of bus 6A and subsequent      
degradation of plant conditions were caused by two equipment             
configuration control problems: the station auxiliary transformer load   
tap changer having been left in the "Manual" position; and the improper  
overcurrent trip setting for emergency diesel generator 23 output        
breaker. In both cases, station personnel failed to ensure the equipment 
configuration was controlled as specified in the licensing and design    
bases. The team also concluded that lapses in management oversight       

HEADQUARTERS      MORNING REPORT     PAGE  2          NOV. 02, 1999
MR Number: H-99-0096 (cont.)

significantly contributed to the event. Station management missed        
significant opportunities to recognize and fully assess degrading plant  
conditions and failed to establish viable plans and contingencies for    
plant restoration.                                                       
                                                                         
The results of the licensee and NRC risk evaluations of this event were  
similar. The risk estimates were conservative in that no credit was given
for "bleed and feed" cooling, the #23 auxiliary feedwater pump was       
considered unrecoverable, and a low probability of success was assigned  
for the operators using the feedwater system to provide make-up to the   
steam generators. Based on these conservative assumptions, the calculated
conditional core damage probability (CCDP) was 2x10-4. The CCDP is used  
to estimate the risk significance of conditions or events.               
                                                                         
                                                                         
Contact:    Ed Goodwin, NRR                                              
            301-415-1154                                                 
            Email:                                          
_