skip navigation links 
 
 Search Options 
Index | Site Map | FAQ | Facility Info | Reading Rm | New | Help | Glossary | Contact Us blue spacer  
secondary page banner Return to NRC Home Page

Morning Report for May 19, 1999

                       Headquarters Daily Report

                         MAY 19, 1999

***************************************************************************
                    REPORT             NEGATIVE            NO INPUT
                    ATTACHED           INPUT RECEIVED      RECEIVED

HEADQUARTERS                           X                   
REGION I                               X                   
REGION II                              X                   
REGION III          X                                      
REGION IV                              X                   
PRIORITY ATTENTION REQUIRED  MORNING REPORT - REGION III  MAY 19, 1999

Licensee/Facility:                     Notification:

Detroit Edison Co.                     MR Number: 3-99-0044
Fermi 2                                Date: 05/18/99
Newport,Michigan                       SRI via telecon                    
Dockets: 50-341
BWR/GE-4                              

Subject: FERMI UNIT 2 MANUALLY SCRAMMED FOLLOWING TRIP OF THE "A"        
         REACTOR RECIRCULATION PUMP                                      


Discussion:

The Fermi 2 nuclear plant was manually shut down by operators following  
the unexpected trip of a reactor recirculation pump. On May 18, 1999,    
while an electrical maintenance individual was replacing a field brush on
the "A" motor generator (MG) set, an electrical wire contacted the center
slip ring on the motor end of the MG set. The resulting ground fault     
caused a generator lockout relay to trip which tripped the "A" reactor   
recirculation pump. Reactor power remained at 97 percent as core flow    
dropped to approximately 40 percent because of the pump trip. This placed
the reactor in the scram region of the Technical Specification power to  
flow map. In accordance with procedures, the operators placed the mode   
switch to the "shutdown" position which scrammed the reactor. All rods   
inserted as expected, no emergency core cooling system equipment actuated
and no safety relief valves lifted in response to the event. All systems 
responded as expected.                                                   

Regional Action:

The resident inspectors responded to the site, and monitored recovery    
activities.                                                              

Contact:  Anton Vegel                (630)829-9620
_