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Morning Report for February 24, 1999

                       Headquarters Daily Report

                         FEBRUARY 24, 1999

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                    REPORT             NEGATIVE            NO INPUT
                    ATTACHED           INPUT RECEIVED      RECEIVED

HEADQUARTERS                           X                   
REGION I                               X                   
REGION II                              X                   
REGION III          X                                      
REGION IV           X                                      
PRIORITY ATTENTION REQUIRED  MORNING REPORT - REGION III  FEB. 24, 1999

Licensee/Facility:                     Notification:

Commonwealth Edison Co.                MR Number: 3-99-0011
Quad Cities 2                          Date: 02/24/99
Cordova,Illinois                       E-Mail                             
Dockets: 50-265
BWR/GE-3                              

Subject: INADVERTENT DRAINDOWN OF ABOUT 6000 GAL. REACTOR WATER TO TORUS 

Discussion:

Unit 2 was in cold shutdown with reactor water temperature at about 144  
degrees Fahrenheit and reactor water level in a band of 90 to 94 inches  
indicated level (normal level during operations is 30 inches indicated.) 
Core cooling was being maintained in a band of 120 to 170 degrees        
Fahrenheit by the "A" loop of shutdown cooing, after being switched from 
the "B" loop at about 00:32 a.m. (CST). At about 01:02 a.m., operators   
noted a decreasing reactor water level, and secured the "2A" residual    
heat removal pump which stopped shutdown cooling operations.             
                                                                         
Water level continued to decrease, but at a much slower rate once the    
pump was secured. Operators then found that the minimum flow valve for   
the "2A" residual heat removal pump was not closed, as required by       
procedure; but was instead fully open with the breaker for the valve     
de-energized. This had allowed a drain path from the reactor, through    
shutdown cooling piping, into the suppression pool. The licensee         
estimated that about 6000 gallons of reactor vessel water were drained to
the suppression pool.                                                    
                                                                         
At 01:55 a.m. operators restored the "2A" loop of shutdown cooling to the
proper lineup and started the "2A" residual heat removal pump. Water     
level had decreased to about 50 inches indicated. Forced circulation     
using a reactor recirculation pump remained in effect throughout the     
event.                                                                   
                                                                         
The licensee began a prompt investigation, and removed the operators from
shift who were responsible for the event. Operators are being sent to the
simulator to review the event and discuss better means of control for    
evolutions in the control room. ComEd management is planning to send a   
corporate led team to the site to assist in the root cause investigation 
of the event.                                                            

Regional Action:

The resident inspectors responded to the control room, ensured plant     
conditions were stable and began a review of the causes for the event and
the licensee's corrective actions.                                       

Contact:  M. Ring                    (630)829-9703
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REGION IV  MORNING REPORT     PAGE  2          FEBRUARY 24, 1999

Licensee/Facility:                     Notification:

Entergy Operations, Inc.               MR Number: 4-99-0006
Arkansas Nuclear 2                     Date: 02/24/99
Russelville,Arkansas                   Licensee Requested NOED            
Dockets: 50-368
PWR/CE                                

Subject: NOTIFICATION OF ENFORCEMENT DISCRETION TO PERMIT STARTUP        

Discussion:

On February 23, 1999, at 9:02 p.m. EST, NRR granted a Notification of    
Enforcement Discretion to permit restart of Arkansas Nuclear One, Unit 2,
from their 13th refueling outage. Specifically, discretion was granted   
from a Technical Specification 3.3.1.1, Action 2, requirement that the   
Channel D neutron detection instrumentation be returned to operable      
status prior to startup. Additionally, discretion was granted from the   
requirements of Technical Specification 3.0.4 that prevented changing    
modes while relying on Action Statement 2. The discretion will remain in 
effect until the licensee's request for an exigent Technical             
Specification amendment is reviewed, authorized, and implemented.        
                                                                         
During the last operating cycle, the reactor protective system Channel D 
wide-range neutron detector string upper detector had failed. Operators  
had placed the affected reactor protective system trips in bypass and    
continued operation as permitted by Technical Specifications. Channel D  
is one of four redundant protective system channels. The Unit 2 plant    
protective system logic is designed for operation as a 2-out-of-3 logic, 
although it is normally operated in a 2-out-of-4 mode. Technical         
Specifications required the licensee to return the failed channel to an  
operable status prior to startup following the next cold shutdown.       
                                                                         
During the current refueling outage, instrumentation and controls        
technicians had installed a spare detector string and performed          
appropriate postmaintenance testing. However, during the plant heatup,   
the middle detector failed to respond properly to the change in neutron  
leakage. The licensee determined that either the detector or associated  
cabling had failed and that no replacement detector string was available.
Therefore, the licensee requested discretion in accordance with          
NUREG 1600, Part 9900, "Technical Guidance," paragraph 2.3.a, because the
three required channels were operable.                                   
                                                                         
Relying on the discretion, licensed operators made the reactor critical  
at 6:35 a.m. this morning.                                               

Regional Action:

Routine resident inspection.                                             

Contact:  David Loveless             (817)860-8161
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