U.S. Nuclear Regulatory Commission
Operations Center
Event Reports For
01/28/2002 - 01/29/2002
** EVENT NUMBERS **
38634 38656 38657
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|Power Reactor |Event Number: 38634 |
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| FACILITY: SAINT LUCIE REGION: 2 |NOTIFICATION DATE: 01/17/2002|
| UNIT: [1] [2] [] STATE: FL |NOTIFICATION TIME: 13:07[EST]|
| RXTYPE: [1] CE,[2] CE |EVENT DATE: 01/17/2002|
+------------------------------------------------+EVENT TIME: 11:45[EST]|
| NRC NOTIFIED BY: KELLY KORTH |LAST UPDATE DATE: 01/28/2002|
| HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |ROBERT HAAG R2 |
|10 CFR SECTION: | |
|APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | |
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+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE
|
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
|2 N Y 100 Power Operation |100 Power Operation |
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EVENT TEXT
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| OFFSITE NOTIFICATION INVOLVING RECOVERED SEA TURTLE FROM INTAKE CANAL
|
| |
| At approximately 1130 EST on 01/17/02, a green sea turtle was retrieved from |
| the intake canal and a determination was made that it was in need of |
| rehabilitation. As required by the Plant's Sea Turtle Permit, the Florida |
| Fish and Wildlife Conservation Commission (FFWCC) was notified at 1145 EST. |
| |
| The licensee notified the NRC Resident Inspector. |
| |
| See EN #38513 for 2001 occurrences. |
| |
| * * * UPDATE ON 1/28/02 @ 1243 BY KORTH TO GOULD * * * |
| |
| At approximately 1115 on 1/28/02 a loggerhead turtle was retrieved from the |
| plant's intake canal. The turtle was determined to be in need of |
| rehabilitation. Per the licensee's turtle permit, the Florida Fish and |
| Wildlife Conservation Commission (FWCC) was notified at 1125. |
| |
| The NRC Resident Inspector was notified. Notified Reg 2 RDO (Ninh) |
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|Fuel Cycle Facility |Event Number: 38656 |
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| FACILITY: WESTINGHOUSE ELECTRIC CORPORATION |NOTIFICATION DATE:
01/28/2002|
| RXTYPE: URANIUM FUEL FABRICATION |NOTIFICATION TIME: 15:45[EST]|
| COMMENTS: LEU CONVERSION (UF6 to UO2) |EVENT DATE: 01/27/2002|
| COMMERCIAL LWR FUEL |EVENT TIME: 21:15[EST]|
| |LAST UPDATE DATE: 01/28/2002|
| CITY: COLUMBIA REGION: 2 +-----------------------------+
| COUNTY: RICHLAND STATE: SC |PERSON ORGANIZATION |
|LICENSE#: SNM-1107 AGREEMENT: Y |SON NINH R2 |
| DOCKET: 07001151 |JOHN HICKEY NMSS |
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| NRC NOTIFIED BY: WILLIAMS | |
| HQ OPS OFFICER: CHAUNCEY GOULD | |
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|EMERGENCY CLASS: NON EMERGENCY | |
|10 CFR SECTION: | |
|NBNL RESPONSE-BULLETIN | |
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EVENT TEXT
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| 24 HOUR 91-01 BULLETIN RESPONSE |
| |
| Reason for Notification |
| |
| At the time of the event, the Team Leader of the Burnable Absorber Expansion |
| System called the cognizant Nuclear Criticality Safety (NCS) engineer to |
| inform him that 113.5 kg of uranium oxide powder had spilled from process |
| equipment into the granulator hood. |
| |
| |
| Summary of Process |
| |
| Dry UO2 powder blended with U3O6 and erbium oxide is processed in a |
| favorable geometry, gravity fed, vertical pipe from a roll compactor down to |
| a granulator. Inside a hood, the granulator feeds down through a flexible |
| tube into a polypak. |
| |
| |
| As Found Condition |
| |
| A summary of the as found conditions is as follows: |
| |
| It had been determined that the granulator screen needed to be replaced, and |
| operations were stopped. |
| |
| When the granulator screen was removed, material in the vertical pipe |
| spilled down onto the bottom of the hood, remaining contained within the |
| hood. |
| |
| The spill was immediately placed into polypaks and telephone notification |
| was made to Nuclear Criticality Safety. |
| |
| |
| Double Contingency Protection |
| |
| Double contingency protection for this situation, which is classified as a |
| spill, is based on control of mass and moderation, and assumes a |
| hemispherical configuration. The mass limit is 50.3 kgU or 57.1 kg UO2; the |
| moderator limit is 32.1 liters of water. It was determined that double |
| contingency protection was lost because the amount of material spilled |
| exceeded the mass limit. |
| |
| Moderation controls remained intact. Double contingency protection was |
| restored in approximately 30 minutes. Therefore the incident requires |
| notification in accordance with Westinghouse Operating License (SNM-107), |
| paragraph 3.7.3 (c.5), in which greater than safe mass is involved, but |
| controls are restored within four hours. |
| |
| |
| Summary of Activity |
| |
| Nuclear Criticality Safety gave permission to resume operations because |
| double contingency protection had been restored. |
| |
| On January 28, 2002, written instructions were issued to erbia operations |
| personnel and training conducted reinforcing that before removal of the |
| screen from the granulator, the material in the vertical process pipe is to |
| be processed into polypaks. |
| |
| Long term corrective actions to prevent the possibility of recurrence will |
| be evaluated as part of apparent cause analysis. |
| |
| |
| Conclusions |
| |
| Loss of double contingency protection did occur, but was restored within |
| approximately 30 minutes. |
| |
| At no time was criticality possible because there was no moderator present. |
| |
| At no time was there any risk to the health or safety of any employee or |
| member of the public. No exposure to hazardous material was involved. |
| |
| It has been determined that this is a safety significant incident in |
| accordance with governing procedures. An apparent cause analysis will be |
| performed. |
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|Power Reactor |Event Number: 38657 |
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| FACILITY: HADDAM NECK REGION: 1 |NOTIFICATION DATE: 01/28/2002|
| UNIT: [1] [] [] STATE: CT |NOTIFICATION TIME: 17:39[EST]|
| RXTYPE: [1] W-4-LP |EVENT DATE: 01/28/2002|
+------------------------------------------------+EVENT TIME: 16:00[EST]|
| NRC NOTIFIED BY: HOUFF |LAST UPDATE DATE: 01/28/2002|
| HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: NON EMERGENCY |CURTIS COWGILL R1 |
|10 CFR SECTION: | |
|APRE 50.72(b)(2)(xi) OFFSITE NOTIFICATION | |
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+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE
|
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N N 0 Decommissioned |0 Decommissioned |
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EVENT TEXT
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| OFFSITE NOTIFICATION OF AN OIL SPILL |
| |
| A spill of approximately 40 gallons of turbine lube oil in the turbine hall |
| occurred with no release to the environment. This amount was in excess of |
| the reportable quantity of 10 gallons, so notification was made to the |
| Connecticut Department of Environmental Protection of the spill. This |
| incident occurred during a decommissioning activities in the turbine hall. |
| |
| The NRC Resident Inspector was notified. |
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