U.S. Nuclear Regulatory Commission
Operations Center
Event Reports For
08/31/2000 - 09/01/2000
** EVENT NUMBERS **
37277 37278 37279 37280 37281
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|Fuel Cycle Facility |Event Number: 37277 |
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| FACILITY: PADUCAH GASEOUS DIFFUSION PLANT |NOTIFICATION DATE: 08/31/2000|
| RXTYPE: URANIUM ENRICHMENT FACILITY |NOTIFICATION TIME: 05:30[EDT]|
| COMMENTS: 2 DEMOCRACY CENTER |EVENT DATE: 08/30/2000|
| 6903 ROCKLEDGE DRIVE |EVENT TIME: 16:10[CDT]|
| BETHESDA, MD 20817 (301)564-3200 |LAST UPDATE DATE: 08/31/2000|
| CITY: PADUCAH REGION: 3 +-----------------------------+
| COUNTY: McCRACKEN STATE: KY |PERSON ORGANIZATION |
|LICENSE#: GDP-1 AGREEMENT: Y |MELVYN LEACH R3 |
| DOCKET: 0707001 |BRIAN SMITH NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: - | |
| HQ OPS OFFICER: STEVE SANDIN | |
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|EMERGENCY CLASS: N/A | |
|10 CFR SECTION: | |
|OCBA 76.120(c)(2)(i) ACCID MT EQUIP FAILS | |
|OCBB 76.120(c)(2)(ii) EQUIP DISABLED/FAILS | |
|OCBC 76.120(c)(2)(iii) REDUNDANT EQUIP INOP | |
| | |
| | |
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EVENT TEXT
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| AREA CONTROL ROOM (ACR) ALARM POWER LOST DUE TO A FAILURE IN THE POWER |
| TRANSFER SWITCH |
| |
| "At 1610 on 08-30-00 the PSS was informed of a C-331 CAAS Cluster J Trouble |
| alarm. Investigation of trouble alarm revealed that C-331 CAAS Horns |
| solenoids had lost DC power. The C-331 ACR DC alarm power was lost due to |
| the failures in the power transfer switch. Contacts fused together and a |
| solenoid failed which allowed the transfer switch to reposition to the mid |
| (no power) position and prevented repositioning to the emergency power |
| position. Since the CAAS horns did not have power, they were unable to |
| perform the intended safety function, rendering the system inoperable for |
| audibility. The system is required to be operable according to TSR 2.4.4.7.b |
| for the current mode of operation. The horns were without power (inoperable) |
| for approximately 30 minutes until the transfer switch was physically forced |
| to the emergency power position. |
| |
| This event is reportable under 10 CFR 76.120(c)(2) as an event in which |
| equipment required by the TSR is disabled or fails to function as designed. |
| |
| The NRC Resident Inspector has been notified of this event. |
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|Other Nuclear Material |Event Number: 37278 |
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| REP ORG: U.S. AIR FORCE |NOTIFICATION DATE: 08/31/2000|
|LICENSEE: U.S. AIR FORCE |NOTIFICATION TIME: 10:15[EDT]|
| CITY: CANNON AFB REGION: 4 |EVENT DATE: 08/30/2000|
| COUNTY: STATE: NM |EVENT TIME: 14:00[MDT]|
|LICENSE#: 42-23539-01AF AGREEMENT: Y |LAST UPDATE DATE: 08/31/2000|
| DOCKET: |+----------------------------+
| |PERSON ORGANIZATION |
| |CHUCK PAULK R4 |
| |BRIAN SMITH |
+------------------------------------------------+ |
| NRC NOTIFIED BY: MAJOR WROBEL | |
| HQ OPS OFFICER: FANGIE JONES | |
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|EMERGENCY CLASS: N/A | |
|10 CFR SECTION: | |
|BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | |
| | |
| | |
| | |
| | |
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EVENT TEXT
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| 4 MISSING EXIT SIGNS CONTAINING TRITIUM |
| |
| The licensee reported that 4 exit signs, 'Safety Sign' by SRB Technologies |
| Inc., each containing 20 curies of tritium, were discovered missing and |
| presumed stolen from building 1245. An investigation is underway and a |
| report will follow in 30 days. |
| |
| The licensee notified NRC R4 (Gaines). |
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|Fuel Cycle Facility |Event Number: 37279 |
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| FACILITY: GLOBAL NUCLEAR FUEL - AMERICAS |NOTIFICATION DATE: 08/31/2000|
| RXTYPE: URANIUM FUEL FABRICATION |NOTIFICATION TIME: 10:55[EDT]|
| COMMENTS: LEU CONVERSION (UF6 TO UO2) |EVENT DATE: 08/31/2000|
| LEU FABRICATION |EVENT TIME: 10:00[EDT]|
| LWR COMMERICAL FUEL |LAST UPDATE DATE: 08/31/2000|
| CITY: WILMINGTON REGION: 2 +-----------------------------+
| COUNTY: NEW HANOVER STATE: NC |PERSON ORGANIZATION |
|LICENSE#: SNM-1097 AGREEMENT: Y |CAUDLE JULIAN R2 |
| DOCKET: 07001113 |BRIAN SMITH NMSS |
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| NRC NOTIFIED BY: ALLEN MABRY | |
| HQ OPS OFFICER: FANGIE JONES | |
+------------------------------------------------+ |
|EMERGENCY CLASS: N/A | |
|10 CFR SECTION: | |
|BAB2 20.2201(a)(1)(ii) LOST/STOLEN LNM>10X | |
|KFIS 70.52(b) LOSS OF SNM/FISSILE | |
| | |
| | |
| | |
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EVENT TEXT
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| 2 SETS OF CALIBRATION SOURCES DISCOVERED MISSING |
| |
| "At 10 AM on August 31, 2000 Global Nuclear Fuel - Americas determined that |
| two sets of instrument calibration sources are missing following a thorough |
| search. Each source set contains four metal disks electroplated with Pu-239, |
| Total activity contained in both source sets is approximately 1.7 |
| microcuries. The sources had been sent to a vendor for calibration |
| re-certification. |
| |
| "The sources were unaccounted for during a routine source inventory at |
| GNF-A. The vendor performing the calibration recertification last accounted |
| for the sources when shipped on August 2, 2000. Records of the common |
| carrier which transported the sources from the vendor to GNF-A indicate the |
| material was shipped as an excepted package limited quantity and delivered |
| to GNF-A on August 7. 2000. The inner packaging and each source are marked |
| with radioactive warning labels. There is no measurable radiation dose rate |
| from this type of package. A search of likely locations at GNFA has been |
| conducted with negative results. |
| |
| "This event is reportable pursuant to 10CFR20.2201, 10CFR70.52 and |
| 10CFR74.11. Efforts to locate the sources continue." |
| |
| The licensee intends to notify New Hanover County, North Carolina State |
| Department of Radiation Protection, and NRC R2(Ayers). |
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|Power Reactor |Event Number: 37280 |
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| FACILITY: SUSQUEHANNA REGION: 1 |NOTIFICATION DATE: 08/31/2000|
| UNIT: [1] [2] [] STATE: PA |NOTIFICATION TIME: 19:42[EDT]|
| RXTYPE: [1] GE-4,[2] GE-4 |EVENT DATE: 08/24/2000|
+------------------------------------------------+EVENT TIME: 08:38[EDT]|
| NRC NOTIFIED BY: FITCH |LAST UPDATE DATE: 08/31/2000|
| HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |PETE ESELGROTH R1 |
|10 CFR SECTION: | |
|AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
|2 N N 0 Startup |0 Startup |
| | |
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EVENT TEXT
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| THE CONTROL ROOM EMERGENCY OUTSIDE AIR SYSTEM(CREOAS) FUNCTION IS DEFEATED |
| WHEN THE CONTROL ROOM SMOKE REMOVAL FANS OPERATE. |
| |
| On August 24, 2000, Susquehanna Unit 1 was Operating at 100% power and Unit |
| 2 was in Mode 2 at 0% power. Operations had placed the Control Structure |
| (CS) Smoke Removal ventilation system in service aligned to the Control Room |
| (CR) and Technical Support Center (TSC) areas to exhaust the foul odor |
| created by welding on the CR ventilation duct as part of modification work. |
| The CS Smoke Removal System was shutdown after personnel noticed a negative |
| differential pressure was created in the CR and TSC areas. This mode of |
| operation existed for 2 hours and 18 minutes. Subsequent review of the event |
| on August 31, 2000 concluded that when the CR Smoke Removal fans operate, |
| they act to defeat the function of the CREOAS fans which are intended to |
| maintain the CS pressure positive. Maintaining a positive pressure in the CS |
| assures that all air entering the CS has passed through the CREOAS filter |
| train (thus assuring no air enters via infiltration). |
| |
| The NRC Resident Inspector was notified. |
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|Power Reactor |Event Number: 37281 |
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| FACILITY: CLINTON REGION: 3 |NOTIFICATION DATE: 08/31/2000|
| UNIT: [1] [] [] STATE: IL |NOTIFICATION TIME: 21:32[EDT]|
| RXTYPE: [1] GE-6 |EVENT DATE: 08/31/2000|
+------------------------------------------------+EVENT TIME: 17:47[CDT]|
| NRC NOTIFIED BY: TIEDEMANN |LAST UPDATE DATE: 08/31/2000|
| HQ OPS OFFICER: CHAUNCEY GOULD +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |MELVYN LEACH R3 |
|10 CFR SECTION: | |
|AIND 50.72(b)(2)(iii)(D) ACCIDENT MITIGATION | |
|NLCO TECH SPEC LCO A/S | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
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EVENT TEXT
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| PLANT ENTERED 72 HOUR LCO ACTION STATEMENT WHEN DIVISION III DIESEL |
| GENERATOR WAS DECLARED INOPERABLE |
| |
| During performance of Fire Protection Surveillance 9337.81 (performs a |
| functional check of the Division Ill Diesel Generator (DG) Carbon Dioxide |
| (CO2) system operation), the Division Ill DG ventilation system tripped |
| during restoration. Electrical Maintenance personnel were performing a |
| functional check of the Division Ill DG room thermal detectors when the |
| panel reset push button was depressed. The anticipated resets did not occur |
| and the decision was made to restore the system to a safe condition. During |
| restoration, a sticking relay prevented restoration of the Division Ill DG |
| ventilation system. The relay has been reset and the ventilation system |
| restored. |
| |
| Division Ill DG was declared INOPERABLE at 1747 and the plant entered LCO |
| 3.8.1. |
| Action B.1- Perform 9082.01 within 1 hour and every 8 hours thereafter. |
| Action B.2- Declare required features supported by Division Ill DG inop when |
| the redundant required features are inop, within 4 hours. |
| Action B.3.1- Determine Operable DG are not inop due to common cause failure |
| within 24 hours - This action -completed. |
| Action B.4- Restore Div 3 DG to Operable within 72 hrs. |
| Division Ill DG was declared OPERABLE at 1813 and the LCO was exited. |
| |
| The NRC Resident Inspector was notified.. |
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