U.S. Nuclear Regulatory Commission
Operations Center
Event Reports For
08/14/2000 - 08/15/2000
** EVENT NUMBERS **
37223 37224 37225
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|Power Reactor |Event Number: 37223 |
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| FACILITY: MCGUIRE REGION: 2 |NOTIFICATION DATE: 08/14/2000|
| UNIT: [1] [] [] STATE: NC |NOTIFICATION TIME: 07:42[EDT]|
| RXTYPE: [1] W-4-LP,[2] W-4-LP |EVENT DATE: 08/14/2000|
+------------------------------------------------+EVENT TIME: 06:58[EDT]|
| NRC NOTIFIED BY: WESLEY HILL |LAST UPDATE DATE: 08/14/2000|
| HQ OPS OFFICER: FANGIE JONES +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |ANNE BOLAND R2 |
|10 CFR SECTION: | |
|AOUT 50.72(b)(1)(ii)(B) OUTSIDE DESIGN BASIS | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 100 Power Operation |100 Power Operation |
| | |
| | |
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EVENT TEXT
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| BOTH TRAINS OF HIGH PRESSURE INJECTION DECLARED INOPERABLE |
| |
| The licensee, in the process of a routine train swap between the 1B nuclear |
| volume control (NV) pump and the 1A NV pump, the 1B discharge check valve |
| did not fully seat. Flow from the 1A NV pump was being returned through the |
| 1B NV pump to the suction header. This could have affected the capability |
| of both of the NV pumps to perform their required actions in the event that |
| high head injection to the reactor coolant system was needed. Both pumps |
| were declared inoperable at 0658 EDT which made the high head injection |
| system inoperable. The discharge valve on the 1B NV pump was shut at 0710 |
| EDT to restore the 1A NV pump to operable. |
| |
| The method to be used to restore the 1B NV pump to operable is being |
| considered. |
| |
| The licensee intends to notify the NRC Resident Inspector. |
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|General Information or Other |Event Number: 37224 |
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| REP ORG: TEXAS DEPARTMENT OF HEALTH |NOTIFICATION DATE: 08/14/2000|
|LICENSEE: TERA - MAR, INC. |NOTIFICATION TIME: 16:55[EDT]|
| CITY: FORT WORTH REGION: 4 |EVENT DATE: 08/14/2000|
| COUNTY: STATE: TX |EVENT TIME: [CDT]|
|LICENSE#: L03157-008 AGREEMENT: Y |LAST UPDATE DATE: 08/14/2000|
| DOCKET: |+----------------------------+
| |PERSON ORGANIZATION |
| |CHUCK PAULK R4 |
| |C.W. (BILL) REAMER NMSS |
+------------------------------------------------+ |
| NRC NOTIFIED BY: JAMES OGDEN | |
| HQ OPS OFFICER: JOHN MacKINNON | |
+------------------------------------------------+ |
|EMERGENCY CLASS: N/A | |
|10 CFR SECTION: | |
|BAB1 20.2201(a)(1)(i) LOST/STOLEN LNM>1000X | |
| | |
| | |
| | |
| | |
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EVENT TEXT
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| AGREEMENT STATE REPORT INVOLVING STOLEN HUMBOLT MODEL 51001 GAUGE |
| |
| "Gauge was stolen from the back of a Company truck while the operator was in |
| a FINA Station at 2910 Loop 12, Dallas, Texas. The driver had not chained |
| the gauge in the truck and had noted the presence of "unsavory" persons |
| that seemed to be following him and were present at the station when he |
| exited his vehicle. When he returned to his vehicle the gauge was missing. |
| He had the keys and the equipment with which to secure the gauge. |
| |
| "The missing gauge is a Humbolt Model 51001, Serial No.: 2692 with 10 |
| millicurie Cs-137 source, Serial No.: 6604GQ and 40 millicurie Am-241 Be |
| source, Serial No.: NJ02854. |
| |
| "The operator has been counseled by the RSO. |
| |
| "Texas License L03157-008. Licensee is located in Fort Worth, Texas." |
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|Power Reactor |Event Number: 37225 |
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| FACILITY: OYSTER CREEK REGION: 1 |NOTIFICATION DATE: 08/15/2000|
| UNIT: [1] [] [] STATE: NJ |NOTIFICATION TIME: 01:45[EDT]|
| RXTYPE: [1] GE-2 |EVENT DATE: 08/15/2000|
+------------------------------------------------+EVENT TIME: 01:40[EDT]|
| NRC NOTIFIED BY: JERE FREEMAN |LAST UPDATE DATE: 08/15/2000|
| HQ OPS OFFICER: FANGIE JONES +-----------------------------+
+------------------------------------------------+PERSON ORGANIZATION |
|EMERGENCY CLASS: N/A |CLIFFORD ANDERSON R1 |
|10 CFR SECTION: | |
|ASHU 50.72(b)(1)(i)(A) PLANT S/D REQD BY TS | |
| | |
| | |
| | |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR| INIT RX MODE |CURR PWR| CURR RX MODE |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1 N Y 86 Power Operation |78 Power Operation |
| | |
| | |
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EVENT TEXT
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| TECHNICAL SPECIFICATION REQUIRED SHUTDOWN DUE TO LOSS OF SECONDARY |
| CONTAINMENT |
| |
| Two reactor building isolation valves (V-28-21 and V-28-22) are not |
| performing their isolation function. The plant is required to be in the |
| shutdown mode by 0704 EDT on 8/15/00 and cold shutdown mode by 0904 EDT on |
| 8/15/00. The valves were discovered at 0304 EDT on 8/14/00 and the licensee |
| has been working on restoring their function. The licensee is continuing to |
| try to restore their function and qualify other valves to perform their |
| function. |
| |
| The licensee notified the NRC Resident Inspector. |
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