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Morning Report for December 16, 1999

                       Headquarters Daily Report

                         DECEMBER 16, 1999

***************************************************************************
                    REPORT             NEGATIVE            NO INPUT
                    ATTACHED           INPUT RECEIVED      RECEIVED

HEADQUARTERS                           X                   
REGION I                               X                   
REGION II                              X                   
REGION III          X                                      
REGION IV                              X                   
PRIORITY ATTENTION REQUIRED  MORNING REPORT - REGION III  DEC. 16, 1999

Licensee/Facility:                     Notification:

Consumers Power Co.                    MR Number: 3-99-0102
Palisades 1                            Date: 12/14/99
Covert,Michigan                        RI Via Telecon                     
Dockets: 50-255
PWR/CE                                

Subject: PALISADES STARTUP FOLLOWING REFUELING OUTAGE                    

Discussion:

The Palisades Nuclear Plant was taken critical at 3:00 p.m. EST on       
December 10, 1999, and the main generator was synchronized to the grid at
approximately 2:23 p.m. EST on December 14, 1999, following a scheduled  
refueling outage. The outage lasted approximately 59 days. Major         
maintenance items completed included: 1) replacing the seal package on   
Primary Coolant Pumps P-50A, P-50C, and P-50D; 2) replacing the motor on 
Primary Coolant Pump P-50D; 3) rebuilding Primary Coolant Pump P-50A; and
4) replacing both low pressure turbines on the main turbine generator.   
                                                                         
In addition to the scheduled activities, several equipment problems      
emerged during the outage necessitating repairs. These included crack    
indications in control rod drive seal housings and hardened grease in    
control rod drive mechanism clutch assembly bearings. Appropriate repairs
were completed for all the emergent issues.                              

Regional Action:

Resident inspectors observed portions of the reactor and plant startup   
activities and will monitor portions of the plant power escalation to    
full power.                                                              

Contact:  Anton Vegel                (630)829-9620
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