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Morning Report for September 17, 1999

                       Headquarters Daily Report

                         SEPTEMBER 17, 1999

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                    REPORT             NEGATIVE            NO INPUT
                    ATTACHED           INPUT RECEIVED      RECEIVED

HEADQUARTERS                                              X
REGION I            X                                      
REGION II                              X                   
REGION III          X                                      
REGION IV                              X                   
PRIORITY ATTENTION REQUIRED  MORNING REPORT - REGION I  SEP. 17, 1999

Licensee/Facility:                     Notification:

Baltimore Gas & Elec Co.               MR Number: 1-99-0033
Calvert Cliffs 1 2                     Date: 09/17/99
Lusby,Maryland                         SRI PC                             
Dockets: 50-317,50-318
PWR/CE,PWR/CE                         

Subject: HURRICANE FLOYD                                                 

Discussion:

During the daylight hours of September 16, 1999, Calvert Cliffs Units 1  
and 2 experienced tropical storm weather associated with Hurricane Floyd,
as the storm passed up the eastern coast of the United States.  Heavy    
rain and high tropical storm winds occurred.  Storm debris, which        
included small fish and grasses, affected the cooling water intake for   
the main turbines on both units, necessitating a power reduction to      
85 percent power on Unit 1 and a preemptive reduction to 90 percent power
on Unit 2.  Safety systems remained operable during the storm.  During   
the morning of September 17, 1999, with debris removed from the main     
condenser waterboxes, reactor power was restored to full power.          

Regional Action:

The resident inspectors are monitoring licensee activities.              

Contact:  Michele Evans              (610)337-5224
          Scott Stewart              (410)586-2626
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REGION I  MORNING REPORT     PAGE  2          SEPTEMBER 17, 1999

Licensee/Facility:                     Notification:

Northeast Utilities                    MR Number: 1-99-0034
Millstone 3                            Date: 09/17/99
Waterford,Connecticut                  RI/telecon                         
Dockets: 50-423
PWR/W-4-LP                            

Subject: MILLSTONE UNIT 3 POWER REDUCTION                                

Discussion:

On September 17, 1999, at approximately 12:00 a.m., Unit 3 control room  
operators decreased power from 100 percent to about 80 percent power. The
power reduction was in response to a lowering main condenser vacuum. The 
causes of the lowering main condenser vacuum were two fold. Hurricane    
Floyd caused an increased ingress of debris into each of the six Unit 3  
main condenser water boxes, decreasing main condenser heat transfer      
efficiency.  In addition, a combination of storm and tide effects caused 
circulating water temperature to rise, decreasing the heat transfer      
capability of the main condenser.  Power is currently being maintained   
between 80 percent and 90 percent, until routine water box cleaning and  
associated system alignment activities are completed.                    
                                                                         
The resident inspectors observed portions of the down power and          
stabilization activities.  No impact was noted on the safety related     
service water system or its attendant heat exchangers.  Because the      
licensee routinely responds to the impacts of circulating water          
temperature and debris on plant operations, backwashing of condenser bays
is routinely performed.  Further licensee recovery activities will be    
monitored through the implementation of the routine resident inspection  
program.                                                                 

Contact:  A. Cerne                   (860)447-3170
          K. Jenison                 (610)337-5244
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REGION I  MORNING REPORT     PAGE  3          SEPTEMBER 17, 1999

Licensee/Facility:                     Notification:

Peco Energy Company                    MR Number: 1-99-0035
Peach Bottom 2 3                       Date: 09/17/99
Philadelphia,Pennsylvania              RI/PC                              
Dockets: 50-277,50-278
BWR/GE-4,BWR/GE-4                     

Subject: POST STORM STATUS AT PEACH BOTTOM - EVENT NOs. 36173, 36179     
Reportable Event Number: 36173                         

Discussion:

On September 16, 1999, as a result of severe weather caused by Hurricane 
Floyd, Peach Bottom experienced three off normal conditions.             
                                                                         
First, Peach Bottom lost power to the technical support center due to a  
fault on the local power distribution line. A one hour non-emergency     
event notification was made to the NRC for a loss of emergency assessment
capability. Power has been restored.                                     
                                                                         
Secondly, power outages caused 22 of the 96 emergency sirens to become   
inoperable. (Refer to Event No. 36179) The number of inoperable emergency
sirens increased during the storm and currently the transmitter for siren
activation is not in service.                                            
                                                                         
Lastly, bearing lube oil temperatures increased in the Unit 2            
recirculation motor-generators due to service water flow restrictions    
from silt buildup in the lube oil cooler following the storm. Power was  
reduced to remove the 2B recirculation pump and motor-generator from     
service and to clean the lube oil cooler. As of 11:00 on                 
September 17, 1999, Unit 2 is operating in single recirculation loop     
operation using the 2A recirculation pump and motor-generator. When the  
2B lube oil cooler is cleaned, PECO plans to restart the 2B recirculation
motor-generator set and recirculation pump and remove the 2A             
recirculation pump and motor-generator from service to clean the 2A lube 
oil cooler. PECO expects to have both lube oil coolers cleaned and both  
recirculation pumps and motor-generators in operation later today. Safety
related equipment was not adversely affected.                            

Contact:  D. Florek                  (610)337-5185
          A. McMurtray               (717)456-7614
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REGION III  MORNING REPORT     PAGE  4          SEPTEMBER 17, 1999

Licensee/Facility:                     Notification:

Combustion Engineering                 MR Number: 3-99-0079
Hematite Fuel Manufact. Facility       Date: 09/15/99
Hematite,Missouri                      Phone call - onsite NRC inspector  
Dockets: 07000036 

Subject: Declaration of an Unusual Event                                 

Discussion:

On the morning of September 15, 1999, the plant management declared an   
Unusual Event following the plant staff's observation of small uranium   
hexafluoride releases from vaporizer piping system valves in the Oxides  
Building. At the time of the releases to the building, the plant staff   
were troubleshooting problems with some of the system valves and were    
attempting to sublime uranium hexafluoride believed to be trapped within 
the isolated piping system. Upon noticing the releases, the plant staff  
evacuated the immediate area of the releases and measures were taken to  
stop the releases. Once the releases were secured, the plant management  
downgraded the event from an Unusual Event Classification. The systems   
are currently secured pending the plant staff's investigation of the     
circumstances which led to the releases.                                 
                                                                         
No injuries were known to have occurred as a result of the isolated      
releases within the vaporizer area. No releases were known to have       
occurred to the environs.                                                

Regional Action:

At the time of the events, the Region III Deputy Regional Administrator, 
the Division of Nuclear Materials Safety Director, and a Region III      
inspector were onsite. Region III management has initiated a special     
inspection in order to understand the causes for the releases and to     
review the emergency response measures undertaken by the licensee as a   
part of the Unusual Event.                                               

Contact:  K. G. O'Brien              (630)829-9603
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