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Morning Report for July 26, 1999

                       Headquarters Daily Report

                         JULY 26, 1999

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                    REPORT             NEGATIVE            NO INPUT
                    ATTACHED           INPUT RECEIVED      RECEIVED

HEADQUARTERS                           X                   
REGION I            X                                      
REGION II                              X                   
REGION III                             X                   
REGION IV                              X                   
PRIORITY ATTENTION REQUIRED  MORNING REPORT - REGION I  JULY 26, 1999

Licensee/Facility:                     Notification:

Duquesne Light Co.                     MR Number: 1-99-0025
Beaver Valley 1 2                      Date: 07/26/99
Shippingport,Pennsylvania              SRI/PC                             
Dockets: 50-334,50-412
PWR/W-3-LP,PWR/W-3-LP                 

Subject: SENIOR MANAGEMENT REORGANIZATION AT BEAVER VALLEY               

Discussion:

On July 23, 1999, Duquesne Light Company (DLC) announced a reorganization
of senior managers.  Effective July 25, Mr. Lew W. Myers will assume the 
newly created position of Executive Vice President (VP) reporting to Mr. 
James E. Cross, President, Generation Group and Chief Nuclear Officer.   
Mr. Kevin L. Ostrowski, Division VP, Nuclear Operations Group and Plant  
Manager will now report to Mr. Myers.  Mr. Myers also retains the title  
of Senior VP of the First Energy Nuclear Operating Company which has     
negotiated to acquire Beaver Valley Units 1 and 2 through an asset       
transfer expected to conclude by December 1999.  Mr. Myers previously    
served in senior nuclear management positions including VP of the Perry  
Nuclear Power Plant and Plant Manager at South Texas Project Unit 1.     

Contact:  P. Eselgroth               (610)337-5234
          D. Kern                    (724)643-2000
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REGION I  MORNING REPORT     PAGE  2          JULY 26, 1999

Licensee/Facility:                     Notification:

Niagara Mohawk Power Corp.             MR Number: 1-99-0026
Nine Mile Point 1                      Date: 07/26/99
Lycoming,New York                      SRI PC                             
Dockets: 50-220
BWR/GE-2                              

Subject: AUTOMATIC SHUTDOWN DURING POST-MAINTENANCE TESTING OF THE       
         TURBINE GENERATOR MECHANICAL PRESSURE REGULATOR                 

Reportable Event Number: 35954                         

Discussion:

At 3:58 p.m. on July 23, 1999, Unit 1 automatically shutdown from 100%   
reactor power on a high flux signal. All safety systems responded as     
designed; however, both motor-driven feedwater pumps tripped on low      
suction pressure following their automatic start. The feedwater pumps    
were promptly restarted by control room operators and functioned properly
for the duration of the event. The licensee is conducting a review of the
feedwater system design to ensure optimum system response to this and    
similar plant transients.                                                
                                                                         
The cause of the high flux signal was large pressure oscillations due to 
the malfunction of the turbine generator mechanical pressure regulator   
(MPR). The maintenance staff was conducting post-work testing on the MPR 
when the regulator malfunctioned. Detailed examination of the MPR over   
the weekend identified the malfunction to be attributed to internal      
contamination of the "bean" control valve (feedback fine adjustment to   
the pressure sensing bellows) with a lubricant.                          
                                                                         
As of 8:00 a.m. this morning, the unit was in Cold Shutdown.             

Regional Action:

The resident inspectors monitored the licensee's recovery efforts and    
plan to review the event root cause determination and corrective actions 
prior to unit restart.                                                   

Contact:  Michele Evans              (610)337-5378
          Gordon Hunegs              (315)342-4041
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