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Morning Report for January 5, 1999

                       Headquarters Daily Report

                         JANUARY 05, 1999

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                    REPORT             NEGATIVE            NO INPUT
                    ATTACHED           INPUT RECEIVED      RECEIVED

HEADQUARTERS                           X                   
REGION I                               X                   
REGION II                              X                   
REGION III                             X                   
REGION IV           X                                      
PRIORITY ATTENTION REQUIRED  MORNING REPORT - REGION IV  JANUARY  5, 1999

Licensee/Facility:                     Notification:

Texas Utilities Electric Co.           MR Number: 4-99-0001
Comanche Peak 2                        Date: 01/04/99
Glen Rose,Texas                        Resident Inspector                 
Dockets: 50-446
PWR/W-4-LP                            

Subject: MANUAL TRIP OF UNIT 2 FOLLOWING A MAIN TURBINE CONTROL FAILURE  

Discussion:

This morning report provides additional information not contained in the 
January 3, 1999, Event Notification (EN#35213).  At approximately        
11:14a.m. (CST) on January 3,1999, the Comanche Peak Steam Electric      
Station, Unit 2, main turbine generator control valves suddenly and      
unexpectedly closed while at 100 percent rated power.  As designed, all  
steam dumps immediately opened and rods automatically stepped in to      
control the reactor coolant system temperature transient.  The reactor   
plant, designed to withstand a 50 percent load rejection, experienced an 
equivalent 80 percent load rejection event.  Shortly after the control   
valves had closed (approximately 5 seconds), the main turbine control    
system began operating as if it had been transferred to the speed control
mode by controlling main generator output to 200 MWe.  The main turbine  
generator speed control mode resulted in the control valves cycling      
between the fully closed position to 3 percent open every few seconds.   
About 9 seconds into the event, one pressurizer power-operated relief    
valve opened for approximately 5 seconds to control the resultant reactor
coolant system pressure increase.  The pressurizer relief tank blowout   
disc remained intact.  As pressurizer level oscillated from the cyclic   
operation of the control valves, reactor coolant system pressure         
continued to slowly decrease.  Pressurizer heaters, Groups B and D,      
failed to automatically energize as designed.                            
                                                                         
After approximately one minute, operators manually tripped Unit 2.  The  
auxiliary feedwater system automatically started when steam generator    
levels dropped following the manual trip.  Other than one redundant      
auxiliary feedwater flow instrument failure, everything operated as      
expected during the trip.  The unit was stabilized in Mode 3, Hot        
Standby.                                                                 
                                                                         
Prior to defining the restart schedule, the licensee plans to determine  
the cause of the main turbine control system failure; implement          
commitments made to the NRC regarding issues found during their review of
NRC Generic Letter 96-01, "Testing of Safety-Related Logic Circuits;" and
complete repairs to the pressurizer backup heaters, the auxiliary        
feedwater flow instrument, and several other minor failures which        
occurred during the transients.                                          

Regional Action:

The resident inspectors are monitoring the licensee's troubleshooting and
recovery efforts.                                                        

Contact:  Joe Tapia                  (817)860-8243
          Anthony T. Gody            (254)891-1500
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