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Morning Report for May 26, 2000

                       Headquarters Daily Report

                         MAY 26, 2000

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                    REPORT             NEGATIVE            NO INPUT
                    ATTACHED           INPUT RECEIVED      RECEIVED

HEADQUARTERS        X                                      
REGION I                               X                   
REGION II                              X                   
REGION III                             X                   
REGION IV           X                                      
PRIORITY ATTENTION REQUIRED  MORNING REPORT - HEADQUARTERS MAY 26, 2000

Licensee/Facility:                     Notification:

Part 21 Database                       MR Number: H-00-0033
Ppg Architectural Finishes             Date: 05/26/00
                                                                          

Subject: Part 21 - Changed formulation of coating                        

Discussion:

VENDOR: PPG Architectural Finishes      NO: mm-13-0                      
                                                                         
DATE OF DOCUMENT: 04/03/00              ACCESSION NUMBER:                
                                                                         
SOURCE DOCUMENT: EN 36861               REVIEWER: REXB, V. Hodge         
                                                                         
On April 3, 2000, the coating vendor PPG Architectural Finishes reported 
that for small quantities of a silicon stainless steel enamel coating    
used inside primary containment, the formulation changed from that which 
was originally supplied. The vendor states that it notified the single   
affected nuclear power utility.                                          
                                                                         
On May 3, 2000, the vendor updated its report (Accession Number          
ML003712384). Since 1987, the vendor supplied exterior silicone stainless
steel enamel coating 8674 to the Catawba, McGuire, and Oconee licensee,  
Duke Energy Company. The licensee used this coating inside containment on
mirror-insulated piping to minimize the potential for paint chip fouling 
of sump pumps. In a postulated design basis accident, such fouling would 
interfere with the emergency core cooling systems used for recovery from 
the accident. The vendor stated that this product was not sold to any    
other nuclear utility for use in containment.                            
                                                                         
In 1980, the vendor's predecessor, Keeler & Long, Inc., conducted design 
basis accident qualification testing on the 8674 coating, concluding that
the product qualified for Coating Service Level I Exposure because it    
disintegrated by powdering, leaving no sizeable pieces of coating to     
interfere with the emergency core cooling systems. Nevertheless, the     
product was not included in the predecessor's quality assurance program  
and the formulation was thus not appropriately controlled.               
                                                                         
Subsequent testing by the licensee indicates that the original           
formulation and several variations of it exhibit large blisters with     
paint chips being delaminated from the substrate. These chips could foul 
sump pumps in a postulated design basis accident.                        
                                                                         
The vendor states that the licensee intends to continue purchasing this  
product for use in containment as a non-qualified coating. The vendor    
states that the mirror-insulation on piping currently coated with this   
product should minimize the potential for paint chip fouling of sump     
pumps.                                                                   
                                                                         
The NRC will post ensuing reports, if any, on this subject on its website
at http://www.nrc.gov/NRC/PUBLIC/PART21/2000.                            

HEADQUARTERS      MORNING REPORT     PAGE  2          MAY 26, 2000
MR Number: H-00-0033 (cont.)

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REGION IV  MORNING REPORT     PAGE  2          MAY 26, 2000

Licensee/Facility:                     Notification:

Nebraska Public Power District         MR Number: 4-00-0015
Cooper 1                               Date: 05/26/00
Brownville,Nebraska                    From RIs                           
Dockets: 50-298
BWR/GE-4                              

Subject: EQUIPMENT QUALIFICATION DEFICIENCIES WITH OKONITE TAPED SPLICES 
         - UPDATE                                                        


Discussion:

On April 10, 2000, Cooper Nuclear Station management informed the        
resident inspectors that drywell temperature profiles during design basis
accidents may exceed their equipment qualification test temperatures.    
Subsequent review by the licensee determined that the overall concern    
with the environmental qualification of drywell equipment was bounded by 
existing test results, as long as all electrical splices were in the     
configuration bounded by the test.  To help confirm the actual           
configuration, on April 14 a licensee electrician and the NRC's resident 
inspector entered the containment to inspect a sample of splices.  The   
electrician and resident inspector observed that, for most of the Okonite
splices observed, the outer tape was unraveling.  A special inspection   
was chartered to review the circumstances surrounding these              
discrepancies.                                                           
                                                                         
After comprehensive review and corrective actions, on May 26 at          
9:58 a.m., operators at Cooper Nuclear Station began plant restart from  
the forced outage. The licensee plans to close the main output breaker   
early on May 27 and restore the facility to normal operation.            
                                                                         
On May 23, licensee management and technical personnel conducted a       
teleconference with the Regional Administrator and members of the        
regional and NRR staffs to discuss the plant's corrective actions and    
readiness to restart. Licensee personnel have replaced all taped         
environmentally qualified splice treatments in the drywell and steam     
tunnel with alternative qualified treatments.  During the licensee's     
evaluations, certain terminal blocks were also replaced.                 

Regional Action:

The special inspection is continuing, in accordance with Inspection      
Procedure 93102.  The inspection team reviewed the extent of the         
condition and the licensee's repair plans and did not identify any       
outstanding safety issues that affect the restart of the unit.           

Contact:  David Loveless             (817)860-8161
          Wayne Sifre                (817)860-8193
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