skip navigation links 
 
 Search Options 
Index | Site Map | FAQ | Facility Info | Reading Rm | New | Help | Glossary | Contact Us blue spacer  
secondary page banner Return to NRC Home Page

Morning Report for April 7, 2000

                       Headquarters Daily Report

                         APRIL 07, 2000

***************************************************************************
                    REPORT             NEGATIVE            NO INPUT
                    ATTACHED           INPUT RECEIVED      RECEIVED

HEADQUARTERS                           X                   
REGION I            X                                      
REGION II                              X                   
REGION III          X                                      
REGION IV                              X                   
PRIORITY ATTENTION REQUIRED  MORNING REPORT - REGION I  APRIL  7, 2000

Licensee/Facility:                     Notification:

Maine Yankee Atomic Power Co.          MR Number: 1-00-0005
Maine Yankee 1                         Date: 04/06/00
Wiscasset,Maine                                                           
Dockets: 50-309
PWR/CE                                

Subject: MAINE YANKEE BEGINS MAJOR COMPONENT REMOVAL FROM CONTAINMENT    

Discussion:

On the morning of April 6, 2000, Maine Yankee initiated removal of the   
100-ton pressurizer from the containment building of its decommissioning 
reactor facility.  The pressurizer was lifted with the containment polar 
crane and lowered to a horizontal position onto a special transporter for
removal through the containment equipment hatch.  This was the first of  
four major components to be removed, with the first of the three steam   
generators scheduled to be removed on April 7 and the remaining two steam
generators to follow in mid-April.  Preparations for removal of the      
pressurizer and steam generators have been conducted for approximately   
the last year.  These activities have included cutting and removing the  
main steam and feedwater lines and isolation valves; removing smaller    
diameter piping, conduit, and cable trays; concrete cutting to remove    
cubicle walls and to widen the equipment hatch; exterior surface         
decontamination; and welding covers on the openings to these components  
where the piping had been removed.   NRC Region I staff inspected these  
activities and evaluated the licensee's certification of the polar crane.
The pressurizer and steam generators will be temporarily stored near the 
fenced border of the industrial security area behind a shield wall       
constructed from the concrete blocks removed during concrete-cutting     
operations.  All four of these components are expected to be shipped to  
the GTS Duratek facility in Memphis,Tennessee on two barge shipments in  
June.  Maine Yankee anticipates issuing a press release on these events  
by early next week.                                                      

Regional Action:

NRC will continue to review Maine Yankee's decommissioning activities as 
part of its routine inspection program.                                  

Contact:  Mark Roberts               (610)337-5094
          Ronald R. Bellamy          (610)337-5200
_
REGION III  MORNING REPORT     PAGE  2          APRIL  7, 2000

Licensee/Facility:                     Notification:

Commonwealth Edison Co.                MR Number: 3-00-0018
Braidwood 1                            Date: 04/06/00
Braceville,Illinois                                                       
Dockets: 50-456
PWR/W-4-LP                            

Subject: Change in status of Braidwood Unit 1                            

Discussion:

Operators at ComEd's Braidwood Station performed a Unit 1 startup        
following an 18 day, 19 hour refueling outage. This is a record for the  
utility. The reactor was taken critical at 7:48 a.m., on April 5, 2000,  
and the turbine-generator was synchronized to the grid at 7:00 p.m., on  
April 5, 2000. The start up was observed by the resident inspectors.     
Significant maintenance activities completed during this outage included 
reactor refueling, main turbine overhaul, reactor coolant pump           
maintenance, digital rod position indication cable replacement,          
replacement of essential service water pumps 1A and 2A suction valves,   
and repair of safety injection system check valves.                      

Regional Action:

This is for information only.                                            

Contact:  Michael Jordan             (630)829-9637
_