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Morning Report for April 5, 2000

                       Headquarters Daily Report

                         APRIL 05, 2000

***************************************************************************
                    REPORT             NEGATIVE            NO INPUT
                    ATTACHED           INPUT RECEIVED      RECEIVED

HEADQUARTERS                           X                   
REGION I                               X                   
REGION II           X                                      
REGION III                             X                   
REGION IV                              X                   
PRIORITY ATTENTION REQUIRED  MORNING REPORT - REGION II  APRIL  5, 2000

Licensee/Facility:                     Notification:

Virginia Power Co.                     MR Number: 2-00-0010
North Anna 1 2                         Date: 04/05/00
Richmond,Virginia                                                         
Dockets: 50-338,50-339
PWR/W-3-LP,PWR/W-3-LP                 

Subject: UNIT 2 MANUAL TRIP ON POWER LOSS TO "C" REACTOR COOLANT PUMP AND
         FAIURE OF UNIT 1 "H" EMERGENCY DIESEL GENERATOR TO START        


Discussion:

This provides information related to NRC reported event numbers 36857 and
36864. On April 4, the Unit 2 reactor was manually tripped from 8 percent
power due to de-energization of a reactor coolant pump. Personnel        
performing a clearance to support work on the SST removed fuses from the 
wrong circuit.  This de-energized the reactor coolant pump. The unit was 
in the process of starting up after an automatic trip on April 3 due to a
ground fault on the power cable from the station service transformer     
(SST). Unit 2 safety-related equipment performed as expected. The 2J     
emergency diesel generator (EDG) started and re-energized its emergency  
bus.                                                                     
                                                                         
On Unit 1 the clearance error resulted in a power loss to the only       
operating reactor coolant pump and the 1H emergency bus.  Unit 1 was in  
mode 5 after core reload during a refueling outage. At the time of the   
event, shutdown cooling was being provided by the A residual heat removal
(RHR) pump which was powered from the 1H emergency bus. When the 1H EDG  
failed to start, the operator manually started the B RHR pump. Shutdown  
cooling was interrupted for approximately 2 minutes. Power was restored  
to its pre-event configuration in less than two hours and the reactor    
coolant pump was restarted.                                              
                                                                         
Inspection of the 1H EDG discovered lube oil on top of all 12 lower      
pistons. Preliminary analysis indicates that the lube oil hydraulically  
locked the engine. The licensee is still investigating the cause of the  
lube oil being on the pistons.                                           

Regional Action:

Routine followup by the resident inspectors.                             

Contact:  L. GARNER                  (404)562-4552
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