skip navigation links 
 
 Search Options 
Index | Site Map | FAQ | Facility Info | Reading Rm | New | Help | Glossary | Contact Us blue spacer  
secondary page banner Return to NRC Home Page

Morning Report for September 6, 2001

                       Headquarters Daily Report

                         SEPTEMBER 06, 2001

***************************************************************************
                    REPORT             NEGATIVE            NO INPUT
                    ATTACHED           INPUT RECEIVED      RECEIVED

HEADQUARTERS                           X                   
REGION I                               X                   
REGION II           X                                      
REGION III                             X                   
REGION IV                              X                   
PRIORITY ATTENTION REQUIRED  MORNING REPORT - REGION II  SEP. 06, 2001

Licensee/Facility:                     Notification:

Tennessee Valley Authority             MR Number: 2-01-0017
Watts Bar 1                            Date: 09/06/01
Spring City,Tennessee                                                     
Dockets: 50-390
PWR/W-4-LP                            

Subject:  MANUAL REACTOR TRIP DUE TO STEAM GENERATOR LEVEL APPROACHING   
          LO-LO LEVEL SETPOINT                                           


Discussion:

The licensee has completed troubleshooting activities and corrective     
actions in response to the September 4, 2001, manual reactor trip.       
Unit 1 achieved criticality at 12:39 a.m., on September 6, 2001.         
                                                                         
The licensee's investigation determined that the loss of normal feedwater
flow to the #1 SG occurred when the #1 SG feedwater regulating valve shut
due to loss of a Vital AC Inverter.  It was determined that an electronic
card failure caused the loss of output from the vital inverter.          
                                                                         
The turbine driven AFW pump did start and inject feedwater into all SGs  
during the event.  The 1A motor driven auxiliary feedwater pump (MDAFW)  
auto started, but did not provide feedwater flow to the SGs because the  
pump discharge pressure control valve failed closed due to the loss of   
power from the vital inverter.  Plant operators secured the pump until   
power was restored to the vital AC bus from a maintenance power supply.  
                                                                         
Additionally, the 1B MDAFW pump did not automatically start, but was     
promptly started by a control room operator.  During subsequent          
troubleshooting, the licensee physically inspected the most likely causes
of the failure of the 1B MDAFW pump to auto start.  In addition the pump 
was successfully stared twice using simulated automatic start signals.   
The licensee also conducted a test which included initiation of a loss of
feedwater pumps actuation signal (same as for the event).  All three AFW 
pumps successfully started.  Despite this review and testing, the        
licensee was unable to determine the cause of the 1B MDAFW auto start    
failure.                                                                 
                                                                         
Reactor power level is currently at 20% and the unit is proceeding to    
full power operations.                                                   

Regional Action:

The residents are monitoring restart activities.                         

Contact:  Paul Fredrickson           (404)562-4530
_
REGION II  MORNING REPORT     PAGE  2          SEPTEMBER  6, 2001

Licensee/Facility:                     Notification:

Duke Power Co.                         MR Number: 2-01-0018
Catawba 1 2                            Date: 09/06/01
York,South Carolina                                                       
Dockets: 50-413,50-414
PWR/W-4-LP,PWR/W-4-LP                 

Subject: MANAGEMENT CHANGES                                              

Discussion:

Duke Energy Corporation announced that Mr. Mike Glover (currently        
Catawba's Operations Superintendent) will succeed Mr. Ron Jones as the   
Station Manager at Catawba.  As previously indicated in Morning Report   
2-01-0014, dated August 16, 2001, Mr. Ron Jones will be assuming the     
position of Station Manager at Oconee as of October 1, 2001.  Mr.        
Glover's successor has not been announced.                               

Regional Action:

For information only.                                                    

Contact:  ROBERT CARROLL             (404)562-4511
_