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Morning Report for May 2, 2001

                       Headquarters Daily Report

                         MAY 02, 2001

***************************************************************************
                    REPORT             NEGATIVE            NO INPUT
                    ATTACHED           INPUT RECEIVED      RECEIVED

HEADQUARTERS        X                                      
REGION I                               X                   
REGION II                              X                   
REGION III                             X                   
REGION IV                              X                   
PRIORITY ATTENTION REQUIRED  MORNING REPORT - HEADQUARTERS MAY 2, 2001

Licensee/Facility:                     Notification:

Union Electric Co.                     MR Number: H-01-0031
Callaway 1                             Date: 05/02/01
Fulton,Missouri                                                           
Dockets: 50-483
PWR/W-4-LP                            

Subject: Callaway Inspection of Main Feedwater Piping Reveals            
         Significant Pipe Wall Thinning                                  


Discussion:

During a Callaway refueling outage that began on April 7, 2001, a        
scheduled inspection to assess the effects of flow-accelerated corrosion 
(FAC) on the main feedwater (MFW) system revealed numerous areas of      
significant degradation. In 1999, following a steam line rupture event,  
the licensee revised how MFW was modeled and upgraded their FAC software 
to Checkworks, Rev. F.                                                   
                                                                         
The inspection of MFW during the current outage was driven by predictions
from the enhanced program. The licensee had anticipated finding          
degradation, but not to the extent observed. In response to their        
findings and additional industry information, the licensee further       
expanded FAC inspections into additional system areas. The results of    
these expanded inspections are not yet available.                        
                                                                         
With regard to MFW, numerous components, primarily 14-inch elbows, in    
both the turbine building and reactor building were found to be degraded 
to below minimum wall thickness or were expected to degrade below minimum
wall thickness prior to the next scheduled outage. These components were 
scheduled for repair or replacement prior to restart. The licensee is    
evaluating why a routine FAC program inspection identified high energy   
piping degraded beyond expectations and in need of extensive unplanned   
repair.                                                                  
                                                                         
This issue is currently being followed by Region IV routine inspection.  
                                                                         
Contacts:   William D. Johnson, R-IV/DRP/RPB                             
            (817) 860-8148                                               
            Email: wdj@nrc.gov                                           
                                                                         
            Ross Telson, NRR/DRIP/REXB                                   
            (301) 415-1175                                               
            Email: rdt@nrc.gov                                           
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