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Morning Report for April 30, 2001

                       Headquarters Daily Report

                         APRIL 30, 2001

***************************************************************************
                    REPORT             NEGATIVE            NO INPUT
                    ATTACHED           INPUT RECEIVED      RECEIVED

HEADQUARTERS                           X                   
REGION I            X                                      
REGION II                              X                   
REGION III                             X                   
REGION IV                              X                   
PRIORITY ATTENTION REQUIRED  MORNING REPORT - REGION I  APRIL 30, 2001

Licensee/Facility:                     Notification:

Northeast Utilities                    MR Number: 1-01-0008
Millstone 2                            Date: 04/29/01
Waterford,Connecticut                                                     
Dockets: 50-336
PWR/CE                                

Subject: AUTOMATIC REACTOR SHUTDOWN DUE TO PERSONNEL ERROR               
Reportable Event Number: 37952                         

Discussion:

On April 29,2001, at 11:28 a.m., Millstone Unit 2 automatically shut down
(turbine and reactor trip) from 97.5% power.  This resulted from a       
partial loss of condenser vacuum.  Personnel error caused an inadvertent 
loss of the "C" circulating water (CW) pump during ongoing work          
supporting the "D" CW pump outage.  The error occurred when an           
electrician disturbed a control circuit in the "D" CW pump breaker       
cubicle that caused the "C" CW pump to trip.                             
                                                                         
Following the automatic reactor trip, all major equipment responded as   
expected, which included actuation of emergency feedwater due to         
post-trip steam generator level change.  Operators stabilized the plant  
condition in Mode 3, at normal operating pressure and temperature.  In   
addition, the steam line atmospheric relief valves lifted momentarily and
reseated as designed following the turbine trip due to the pressure      
transient in the secondary plant.  Contrary to the information in the    
subject event notification report, the steam generator safety valves did 
not lift during this event.  The licensee is conducting maintenance on   
selected plant systems which they expect to complete later today.        
                                                                         
RI responded to site to review licensee actions.                         

Contact:  R. Summers                 (610)337-5282
          C. Cowgill                 (610)337-5233
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