skip navigation links 
 
 Search Options 
Index | Site Map | FAQ | Facility Info | Reading Rm | New | Help | Glossary | Contact Us blue spacer  
secondary page banner Return to NRC Home Page

Morning Report for March 2, 2001

                       Headquarters Daily Report

                         MARCH 02, 2001

***************************************************************************
                    REPORT             NEGATIVE            NO INPUT
                    ATTACHED           INPUT RECEIVED      RECEIVED

HEADQUARTERS                           X                   
REGION I                               X                   
REGION II           X                                      
REGION III                             X                   
REGION IV                              X                   
PRIORITY ATTENTION REQUIRED  MORNING REPORT - REGION II  MARCH  2, 2001

Licensee/Facility:                     Notification:

Duke Power Co.                         MR Number: 2-01-0003
Oconee 3                               Date: 03/02/01
Seneca,South Carolina                                                     
Dockets: 50-287
PWR/B&W-L-LP                          

Subject: PRESSURE BOUNDARY LEAKAGE - OCONEE UNIT 3 (UPDATE)              

Discussion:

This is an update to Event Report Number 37760. On February 17, 2001,    
Oconee Unit 3 performed a planned shutdown to replace a leaking          
(approximately 1.5 gallon per minute) pressurizer code safety relief     
valve. Following the shutdown, visual inspections of the reactor vessel  
head revealed evidence of boron buildup around six control rod drive     
mechanisms (CRDMs). The licensee performed these inspections due to      
similar indications of pressure boundary leakage found during the most   
recent Unit 1 outage (see Event Report Number 37567).                    
                                                                         
Currently, Unit 3 remains fueled with the reactor vessel head removed to 
facilitate non-destructive examinations. Although the results of the     
examinations are still under review, one or more axial indications have  
been identified thus far in each of the six CRDM vessel head nozzles.    
Three additional CRDM nozzles which had some indications of boron at the 
head area also received non-destructive examination. The preliminary     
examination results identified indications in these nozzles. The licensee
is developing plans to examine a representative sample of the remaining  
CRDM nozzles.                                                            

Regional Action:

A conference call between the NRC and the licensee was held on March 1,  
2001, to discuss the licensee's current examination results, status of   
their root cause investigation, and proposed repair plans. An additional 
conference call will be held when more definitive examination results are
available. The resident inspectors, along with the Region and NRR, will  
continue to monitor the licensee's recovery actions.                     

Contact:  ROBERT HAAG                (404)562-4550
_