![]() |
Search Options | |||
Index | Site Map | FAQ | Facility Info | Reading Rm | New | Help | Glossary | Contact Us | ![]() |
ACCESSION #: 9606260244 South Carolina Electric & Gas Company Gary J. Taylor P. O. Box 88 Vice President Jenkinsville, SC 29065 Nuclear Operations (803) 345-4344 SCE&G A SCANA Company June 17, 1996 RC-96-0157 Document Control Desk U. S. Nuclear Regulatory Commission Washington, DC 20555 Gentlemen: Subject: VIRGIL C.SUMMER NUCLEAR STATION(VCSNS) DOCKET NO. 50/395 OPERATING LICENSE NO. NPF-12 INTERIM PART 21 REPORT (SSH 960004) South Carolina Electric & Gas Company (SCE&G) submits this letter in accordance with 10CFR21.21(a)(2) as an interim report of an identified defect potentially associated with a substantial safety hazard. On April 28, 1996, Nonconformance Notice (NCN) 5415 was initiated to address the nozzle weld defects in the Chemical and Volume Control System connections at the reactor coolant pump seal injection line nozzles and Component Cooling Water System connections at the reactor coolant pump thermal barrier heat exchanger inlet and outlet nozzles. The subject condition appears to be a generic hardware defect in manufacturing. SCE&G suspects that weld flaws existed in the original nozzle welds supplied by Westinghouse. SCE&G has taken the following actions: All nine (9) nozzles were inspected. Six (6) nozzles revealed indications of cracking and were repaired using the TIG welding process, and satisfactorily reinspected. The original equipment manufacturer has been contacted. SCE&G expects to complete the evaluation of 10CFR21 reportability prior to September 1, 1996. If you require any further information, please contact Mr. Michael J. Zaccone at (803) 345-4328. Very truly yours, Gary J. Taylor MJZ/GJT/nkk c: J. L. Skolds J. B. Knotts, Jr. R. R. Mahan NSRC R. J. White DMS (RC-96-0157) S. D. Ebneter RTS (SSH 960004) A. R. Johnson File (818.18) NRC Resident Inspector NUCLEAR EXCELLENCE - A SUMMER TRADITION! *** END OF DOCUMENT ***