skip navigation links 
 
 Search Options 
Index | Site Map | FAQ | Facility Info | Reading Rm | New | Help | Glossary | Contact Us blue spacer  
secondary page banner Return to NRC Home Page

Event Notification Report for July 1, 2003



                    U.S. Nuclear Regulatory Commission
                              Operations Center

                              Event Reports For
                           06/30/2003 - 07/01/2003

                              ** EVENT NUMBERS **

39958  39965  39966  39967  39968  39969  39970  



+------------------------------------------------------------------------------+
|General Information or Other                     |Event Number:   39958       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| REP ORG:  NC DIV OF RADIATION PROTECTION       |NOTIFICATION DATE: 06/25/2003|
|LICENSEE:  BARNHILL CONTRACTING COMPANY         |NOTIFICATION TIME: 10:45[EDT]|
|    CITY:  CHAPEL HILL              REGION:  2  |EVENT DATE:        06/25/2003|
|  COUNTY:                            STATE:  NC |EVENT TIME:        10:20[EDT]|
|LICENSE#:                        AGREEMENT:  Y  |LAST UPDATE DATE:  06/26/2003|
|  DOCKET:                                       |+----------------------------+
|                                                |PERSON          ORGANIZATION |
|                                                |CHARLES R. OGLE      R2      |
|                                                |DOUG BROADDUS        NMSS    |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  SHARN JEFFRIES               |                             |
|  HQ OPS OFFICER:  STEVE SANDIN                 |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          NON EMERGENCY         |                             |
|10 CFR SECTION:                                 |                             |
|NAGR                     AGREEMENT STATE        |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| DAMAGED TROXLER DENSITY GAUGE                                                |
|                                                                              |
| At 1020 EDT on 6/25/03, the NC Radiation Protection Section was notified     |
| that a portable nuclear gauge being used was run over by a passenger van at  |
| the intersection of Faivon and Bucchaneer Roads (near Hwy 40 and the 55      |
| interchange).  The Authorized User is on site and has the gauge cordoned off |
| as per emergency procedures require.  The van involved in the collision is   |
| being detained..  Both the RSO and Alt RSO are enroute to perform surveys (1 |
| hour).                                                                       |
|                                                                              |
| NC Radiation Protection Section personnel are responding to the scene to     |
| perform surveys (30 mins).                                                   |
|                                                                              |
| The device is described as a Troxler Gauge containing 8 millicuries Cs-137.  |
| NC Incident Report No.: 03-27.                                               |
|                                                                              |
| * * * UPDATE 0952 EDT ON 6/26/03 FROM NC RAD PROTECTION VIA FAX * * *        |
|                                                                              |
| The following additional information was provided by NC:                     |
|                                                                              |
| Incident Location: Chapel Hill, NC . Intersection of Faison and Buckner      |
| Roads. Take 40 West from Raleigh to the NC54 exit towards Chapel Hill. Take  |
| a right onto Meadowmont, then a left onto Sprunt. Follow Sprunt to Weaver    |
| Lane and take a right onto Weaver Lane. Take a right on Faison off of Weaver |
| lane, go downhill to the intersection of Faison and Buckner.                 |
|                                                                              |
| Brief Description of Incident: Paving contractor in a commercial van was not |
| watching where he was driving and ran over the instrument panel part of a    |
| Troxler model 4640B thin lift density gauge. The licensee was performing a   |
| standardization count on the gauge at the time of the accident so the source |
| was in the shielded position when it was run over. The gauge was pushed off  |
| the standardization plate and dragged about 3 feet. The gauge then rolled    |
| onto it's side and the source handle was shoved into the asphalt. The        |
| licensee stopped the van and detained it and the driver until the gauge      |
| could be surveyed and it was determined that there were no loose source or   |
| contamination concerns. The area was cordoned off with pink surveyors' tape  |
| and controlled until the gauge and accident area was surveyed and the gauge  |
| returned to the Troxler shipping container. Survey results of the gauge done |
| by both the licensee and the NCDENR RAM Branch were consistent with an       |
| undamaged gauge. The licensee placed the gauge into the Troxler              |
| transportation case for delivery to Troxler for leak testing and servicing.  |
| The damage appears to be cosmetic with some damage to be expected to the     |
| electronics.                                                                 |
|                                                                              |
| Radiological Information: Isotope(s): Cesium-137, Activity: 8 millicuries,   |
| Device: Troxler Gauge, model 4640B                                           |
|                                                                              |
| Notified R2DO (C. Ogle) and NMSS (Broaddus).                                 |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   39965       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: COLUMBIA GENERATING STATIREGION:  4  |NOTIFICATION DATE: 06/30/2003|
|    UNIT:  [2] [] []                 STATE:  WA |NOTIFICATION TIME: 14:39[EDT]|
|   RXTYPE: [2] GE-5                             |EVENT DATE:        06/30/2003|
+------------------------------------------------+EVENT TIME:        09:18[PDT]|
| NRC NOTIFIED BY:  SCOTT BURTON                 |LAST UPDATE DATE:  06/30/2003|
|  HQ OPS OFFICER:  HOWIE CROUCH                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |CHARLES MARSCHALL    R4      |
|10 CFR SECTION:                                 |                             |
|ARPS 50.72(b)(2)(iv)(B)  RPS ACTUATION - CRITICA|                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|2     A/R        Y       79       Power Operation  |0        Hot Shutdown     |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| VALID REACTOR PROTECTION SYSTEM ACTUATION                                    |
|                                                                              |
| The following information was obtained from the licensee via facsimile:      |
|                                                                              |
| "This event notification is being made to report the valid actuation of the  |
| reactor protection system when the reactor was critical, and subsequent      |
| reactor scram.  On June 30, 2003, [at 0918 PDT], the plant was in Mode 1 at  |
| 79% power, when a turbine trip occurred, followed by a reactor scram.  The   |
| cause of the turbine trip is unknown at this time.  All plant systems        |
| functioned properly in response to the scram.  Operators are proceeding to   |
| bring the plant to Mode 4, Cold Shutdown, while investigation into the cause |
| of the transient is completed."                                              |
|                                                                              |
| During the scram, all rods inserted into the core.  There were no lifts of   |
| power-operated or manual relief valves during the transient.  The electrical |
| grid is stable and powering all safety equipment.  There were no other       |
| specified system actuations.  Decay heat is being removed via the bypass     |
| valves to the main condenser.                                                |
|                                                                              |
| The licensee has informed the NRC Resident Inspector.                        |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   39966       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: PERRY                    REGION:  3  |NOTIFICATION DATE: 06/30/2003|
|    UNIT:  [1] [] []                 STATE:  OH |NOTIFICATION TIME: 15:54[EDT]|
|   RXTYPE: [1] GE-6                             |EVENT DATE:        06/30/2003|
+------------------------------------------------+EVENT TIME:        15:41[EDT]|
| NRC NOTIFIED BY:  DAVE BLOUNT                  |LAST UPDATE DATE:  06/30/2003|
|  HQ OPS OFFICER:  HOWIE CROUCH                 +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |BRENT CLAYTON        R3      |
|10 CFR SECTION:                                 |TIM MCGINTY          IRO     |
|AAEC 50.72(a) (1) (i)    EMERGENCY DECLARED     |BOB DENNIG           NRR     |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| UNUSUAL EVENT DECLARED DUE TO SEISMIC EVENT IN THE AREA                      |
|                                                                              |
| At 1541 EDT on 6/30/03,  Perry Nuclear Plant declared an Unusual Event due   |
| to a seismic event.  No immediate issues were noticed.  The operating-basis  |
| earthquake/safe-shutdown annunciator did not alarm, however the plant did    |
| receive a seismic panel alarm.  The set point for the alarm is 0.005g.       |
| There were no unplanned radioactive releases.  No protective action          |
| recommendations are advised by the licensee.  State and local counties       |
| (Lake, Geauga and Ashtabula) have been informed.                             |
|                                                                              |
| The National Earthquake Information Center has preliminary indications that  |
| the earthquake measured 3.4 on the Richter scale at 41.7 N latitude and 81.2 |
| W longitude near Painesville, OH.                                            |
|                                                                              |
| The licensee has notified the NRC Resident Inspector                         |
|                                                                              |
| * * *  UPDATE AT 2242 ON 06/30/03 CARMAN TO GOTT * * *                       |
|                                                                              |
| Licensee terminated from unusual event.  Action needed to terminate from the |
| unusual event was a plant walk down.  The licensee completed same with no    |
| plant damage identified, no unplanned radiological release, and no planned   |
| corrective actions.                                                          |
|                                                                              |
| The licensee notified the NRC Resident and Senior Resident Inspectors.       |
|                                                                              |
| Notified NRR EO (Ruland), DIRO Manager (McGinty), DHS (Murray), FEMA         |
| (Stiendurf), and R3DO (Clayton)                                              |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   39967       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: SEABROOK                 REGION:  1  |NOTIFICATION DATE: 06/30/2003|
|    UNIT:  [1] [] []                 STATE:  NH |NOTIFICATION TIME: 17:20[EDT]|
|   RXTYPE: [1] W-4-LP                           |EVENT DATE:        06/30/2003|
+------------------------------------------------+EVENT TIME:        14:59[EDT]|
| NRC NOTIFIED BY:  RON STRICKLAND               |LAST UPDATE DATE:  06/30/2003|
|  HQ OPS OFFICER:  BILL GOTT                    +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |RICHARD BARKLEY      R1      |
|10 CFR SECTION:                                 |DIANE SCRENCI        R1PA    |
|APRE 50.72(b)(2)(xi)     OFFSITE NOTIFICATION   |WILLIAM BEECHER      PAO     |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| OFFSITE NOTIFICATION DUE TO FIRE                                             |
|                                                                              |
| "At 1459 EDT 06/30/03 a fire was reported on Unit II containment.  The fire  |
| was on wooden staging, and was about the size of a normal campfire.  The     |
| fire was a result of the disassembly of the Unit II containment dome.  Per   |
| procedure, the Seabrook Fire Department was called and responded.  The fire  |
| was extinguished by the Unit II disassembly crew (the onsite fire brigade    |
| did not respond because the fire was outside of the Unit I protected area).  |
| The Seabrook Fire Department was not used to extinguish the fire.  Corporate |
| Communications Group have been in contact with Channel 9 and with the        |
| Associated Press.  The fire was extinguished at 1535 using prestaged hoses.  |
| The fire water was provided by Hydrant #15 of Seabrook Station's Fire        |
| Protection System."                                                          |
|                                                                              |
| The NRC Resident Inspector was notified.                                     |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   39968       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: BRUNSWICK                REGION:  2  |NOTIFICATION DATE: 06/30/2003|
|    UNIT:  [1] [] []                 STATE:  NC |NOTIFICATION TIME: 17:30[EDT]|
|   RXTYPE: [1] GE-4,[2] GE-4                    |EVENT DATE:        06/30/2003|
+------------------------------------------------+EVENT TIME:        17:10[EDT]|
| NRC NOTIFIED BY:  D. W. BAIN                   |LAST UPDATE DATE:  06/30/2003|
|  HQ OPS OFFICER:  ERIC THOMAS                  +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |CHARLES R. OGLE      R2      |
|10 CFR SECTION:                                 |                             |
|ASHU 50.72(b)(2)(i)      PLANT S/D REQD BY TS   |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       93       Power Operation  |92       Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| TECH SPEC REQUIRED SHUTDOWN                                                  |
|                                                                              |
| On June 30, 2003, at 1710 EDT, Unit 1 reactor power was decreased,           |
| initiating a reactor shutdown required by                                    |
| Technical Specification (TS) Limiting Condition for Operation (LCO) 3.4.4    |
| due to Reactor Coolant System (RCS)                                          |
| operational leakage exceeding a TS LCO limit.  At 0615 hours, TS LCO 3.4.4   |
| was entered due to an increase in                                            |
| unidentified leakage of greater than 2 gpm (gallons per minute) within the   |
| previous 24 hour period.  Leakage increased from 0.63 gpm on June 29, 2003   |
| at 2000 EDT, to 2.69 gpm on June 30, 2003 at 0615 EDT.  Required Actions     |
| from LCO 3.4.4 are to reduce leakage to within TS limits within 8 hours or   |
| be in Mode 3 (Hot Shutdown) in 12 hours and Mode 4 (Cold Shutdown) in 36     |
| hours.  As of 1700 EDT, leakage could not be reduced to exit the TS LCO      |
| Condition.                                                                   |
|                                                                              |
| The licensee notified the NRC Resident Inspector.                            |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Research Reactor                                 |Event Number:   39969       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: MASSACHUSETTS INSTITUTE OF TECH      |NOTIFICATION DATE: 06/30/2003|
|   RXTYPE: 5000 KW TANK RESEARCH HW             |NOTIFICATION TIME: 17:44[EDT]|
| COMMENTS:                                      |EVENT DATE:        06/30/2003|
|                                                |EVENT TIME:        06:45[EDT]|
|                                                |LAST UPDATE DATE:  06/30/2003|
|    CITY:  CAMBRIDGE                REGION:  1  +-----------------------------+
|  COUNTY:  MIDDLESEX                 STATE:  MA |PERSON          ORGANIZATION |
|LICENSE#:  R-37                  AGREEMENT:  N  |RICHARD BARKLEY      R1      |
|  DOCKET:  05000020                             |ALEXANDER ADAMS      NRR     |
+------------------------------------------------+                             |
| NRC NOTIFIED BY:  JOHN BERNARD                 |                             |
|  HQ OPS OFFICER:  BILL GOTT                    |                             |
+------------------------------------------------+                             |
|EMERGENCY CLASS:          NON EMERGENCY         |                             |
|10 CFR SECTION:                                 |                             |
|NINF                     INFORMATION ONLY       |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
|                                                |                             |
+------------------------------------------------------------------------------+

                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| OPERATOR ASLEEP AT REACTOR CONTROLS                                          |
|                                                                              |
| The following was emailed from the licensee to the NRC Project Manager:      |
|                                                                              |
| "The licensee Facility Director called the NRC project manager to report     |
| that on 6/29/03 between 0605 EDT and 0645, the operator at the control       |
| console fell asleep for approximately 25 minutes.  The operator had logged   |
| console operations at 0605 and 0645.  Other licensee personnel had tried to  |
| contact the console operator during this time period without success.  The   |
| licensee is investigating the event and will review this situation with all  |
| reactor operators."                                                          |
|                                                                              |
| This is in violation of 10 CFR 50.54 (k).                                    |
+------------------------------------------------------------------------------+

+------------------------------------------------------------------------------+
|Power Reactor                                    |Event Number:   39970       |
+------------------------------------------------------------------------------+
+------------------------------------------------------------------------------+
| FACILITY: MONTICELLO               REGION:  3  |NOTIFICATION DATE: 07/01/2003|
|    UNIT:  [1] [] []                 STATE:  MN |NOTIFICATION TIME: 00:04[EDT]|
|   RXTYPE: [1] GE-3                             |EVENT DATE:        06/30/2003|
+------------------------------------------------+EVENT TIME:        15:45[CDT]|
| NRC NOTIFIED BY:  DAVID BARNETT                |LAST UPDATE DATE:  07/01/2003|
|  HQ OPS OFFICER:  MIKE RIPLEY                  +-----------------------------+
+------------------------------------------------+PERSON          ORGANIZATION |
|EMERGENCY CLASS:          NON EMERGENCY         |BRENT CLAYTON        R3      |
|10 CFR SECTION:                                 |                             |
|AINA 50.72(b)(3)(v)(A)   POT UNABLE TO SAFE SD  |                             |
|AINB 50.72(b)(3)(v)(B)   POT RHR INOP           |                             |
|AINC 50.72(b)(3)(v)(C)   POT UNCNTRL RAD REL    |                             |
|AIND 50.72(b)(3)(v)(D)   ACCIDENT MITIGATION    |                             |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|UNIT |SCRAM CODE|RX CRIT|INIT PWR|   INIT RX MODE  |CURR PWR|  CURR RX MODE   |
+-----+----------+-------+--------+-----------------+--------+-----------------+
|1     N          Y       100      Power Operation  |100      Power Operation  |
|                                                   |                          |
|                                                   |                          |
+------------------------------------------------------------------------------+
                                   EVENT TEXT                                   
+------------------------------------------------------------------------------+
| HIGH ENERGY LINE BREAK (HELB) DOOR NOT LATCHED                               |
|                                                                              |
| "On June 30, 2003 at approximately 1545 [CDT] it was identified that a High  |
| Energy Line Break (HELB) door separating Divisional Motor Control Centers    |
| was not latched as required.  It was determined that this condition existed  |
| for a maximum of 15 minutes.  This condition is being reported as an event   |
| or condition that could have prevented the fulfillment of a safety function  |
| in accordance with 10 CFR 50.72(b)(3)(v)."                                   |
|                                                                              |
| The licensee notified the NRC Resident Inspector and the State Emergency     |
| Management Agency.                                                           |
+------------------------------------------------------------------------------+